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B-737 Cargo Plane down in Hawaii

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B-737 Cargo Plane down in Hawaii

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Old 5th Nov 2021, 11:31
  #281 (permalink)  
 
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Sully's wasn't gentle either. As against recommended ditching of minimum VS, Sully landed around 740ft/mt. That's because of the time pressure his speed went19kts below recommended Vapp and due to activation of airbus alpha (low speed) protection was unable to flare sufficiently. That's why aircraft was written off.

Last edited by vilas; 5th Nov 2021 at 12:26.
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Old 5th Nov 2021, 13:12
  #282 (permalink)  
 
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Any airliner that goes into salt water is going to be a write off. Almost certainly the same for fresh water.
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Old 6th Nov 2021, 11:28
  #283 (permalink)  

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I see TE flaps in, or almost so.

Imagine a crew trying to make a field with insufficient thrust, understandably they'd be keeping clean conf. and speed for max L/D. On the other hand, a pre-determined ditching is surely flown at the slowest Vref you could get.

Estimating 210 and 130 kts for the two cases, with an impact weight of 49 t,

the kinetic energy equation gives 270 MJ and 104 MJ respectively.

No need to look any further why the same metal buckles and bends once but breaks and tears on a different day.

The involuntary ditchings discussed above were all at approach speed, to my understanding.

Last edited by FlightDetent; 6th Nov 2021 at 18:36.
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Old 19th Apr 2022, 11:43
  #284 (permalink)  
 
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Any more news on cause?
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Old 20th Dec 2022, 20:03
  #285 (permalink)  
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Updated report from NTSB is suggesting a human factors accident.
Crew misidentified the dead engine. Crew reported they had lost #1 engine.

https://data.ntsb.gov/Docket/Documen...Docket-Rel.pdf

As the aircraft passed through about 390 ft at 155 knots, engine 2 EPR suddenly dropped to 1.43, while engine 1 remained at its previously set takeoff power. Immediately after engine 2 EPR dropped, the rudder pedal moved to about 5.5 degrees of left rudder, consistent with a command to counteract the adverse yaw of losing thrust on the right engine. The climb paused at 1,000 feet for 25 seconds, then continued to 2,000 ft.

At 2,000 feet, engine 1 EPR reduced to a value of 1.051, which is consistent with idle power in previous flights. It stayed at this value for the remainder of the flight.

Engine 2 EPR also reduced at 2,000 feet, however it continued to be advanced and reduced several times until the end of the flight.

Altitude and airspeed decreased over the next 9 minutes until the end of the recording. At the end of the recording, engine 2 EPR was 1.462 and engine 1 EPR, having been stable since it reduced at 2,000 feet, was still consistent with previous flight idle settings at 1.052.
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Old 21st Dec 2022, 09:48
  #286 (permalink)  
 
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The CVR transcript is certainly illuminating.

https://data.ntsb.gov/Docket?ProjectID=103407
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Old 21st Dec 2022, 15:08
  #287 (permalink)  
 
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Originally Posted by BewareOfTheSharklets
The CVR transcript is certainly illuminating.

https://data.ntsb.gov/Docket?ProjectID=103407
Initially identified correctly by the copilot, who was flying, as the #2 engine. Once more stabilized, probably at a reduced thrust setting, the both pilots appeared to mis-identify the faulty engine as the #1(use of EGT for identification was discussed). It appears that the #1 thrust lever was brought back to idle. Therefore, it could have easily been used when maintaining proper speed/altitude became difficult. Even if you think that engine is faulty, you definitely want to try using it when it becomes obvious that you will be descending into the water soon.

Last edited by punkalouver; 21st Dec 2022 at 15:18.
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Old 21st Dec 2022, 15:10
  #288 (permalink)  
 
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Originally Posted by GBO
“As the aircraft passed through about 390 ft at 155 knots, engine 2 EPR suddenly dropped to 1.43, while engine 1 remained at its previously set takeoff power. Immediately after engine 2 EPR dropped, the rudder pedal moved to about 5.5 degrees of left rudder, consistent with a command to counteract the adverse yaw of losing thrust on the right engine. The climb paused at 1,000 feet for 25 seconds, then continued to 2,000 ft.
Would the rudder deflection have been commanded by pilot foot or yaw damper at this point in the flight?
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Old 21st Dec 2022, 17:09
  #289 (permalink)  
 
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I am reminded of the Kegworth 737 crash where the good engine was also shut down.

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Old 21st Dec 2022, 17:51
  #290 (permalink)  
 
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Originally Posted by BFSGrad
Would the rudder deflection have been commanded by pilot foot or yaw damper at this point in the flight?
On a 737-200??? Or any 737 for that matter. Foot.
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Old 21st Dec 2022, 20:06
  #291 (permalink)  
 
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Originally Posted by RatherBeFlying
I am reminded of the Kegworth 737 crash where the good engine was also shut down.

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IIRC also the TransAsia ATR72 after T/O at Taipei...bad engine rolling, good engine cut
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Old 21st Dec 2022, 22:07
  #292 (permalink)  
 
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Excerpt from the 2nd captain interview. Epiphany?

Oh, if the number 1 engine is gone, it's not only the EPR. Then you'll get backup information. It's not going to be only from Greg [FO]. You're going to get backup indication to confirm that number 1 is gone. But we didn't get there. We didn't, we didn't get there. You know, right now I think, as I'm sitting here and you're asking me about number 1 thrust lever, number 1 -- number 1, I'm beginning to wonder did we shut down the wrong engine, you know? Because I don't know.
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Old 21st Dec 2022, 23:08
  #293 (permalink)  
 
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Is this going to have any imapct on the 737 Max-10 debacle (not that I understand it even vaguely well enough), but isn't the issue they're trying for the ability ignore the mandate on EICAS implementation. I'm an Airbus guy, ECAM or equivalent have identified this far better, certainly far more methodically?

Last edited by giggitygiggity; 22nd Dec 2022 at 01:07.
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Old 22nd Dec 2022, 03:29
  #294 (permalink)  

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There has been a case on Airbus where N1/N2 vibration was mistaken for left/right engine designation. Just because of the digit (while squarely showing on-side where the problem actually was).

Engineering HF mistakes out is understandable, but to which extent is it justified?
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Old 22nd Dec 2022, 17:17
  #295 (permalink)  
 
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Originally Posted by giggitygiggity
Is this going to have any imapct on the 737 Max-10 debacle (not that I understand it even vaguely well enough), but isn't the issue they're trying for the ability ignore the mandate on EICAS implementation. I'm an Airbus guy, ECAM or equivalent have identified this far better, certainly far more methodically?
Actually, the Kegworth disaster would suggest that changing the flight deck from what the crews are used to might be a bad idea. One of the contributing factors in Kegworth was that on the 737-400 (and -300 IIRC) they'd changed the vibration displays relative to the -200 that they crew was used to. That contributed to the crew miss-identifying the bad engine.
Unintended consequences can be a bitch...
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Old 23rd Dec 2022, 01:34
  #296 (permalink)  
 
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Originally Posted by tdracer
Actually, the Kegworth disaster would suggest that changing the flight deck from what the crews are used to might be a bad idea. One of the contributing factors in Kegworth was that on the 737-400 (and -300 IIRC) they'd changed the vibration displays relative to the -200 that they crew was used to. That contributed to the crew miss-identifying the bad engine.
Unintended consequences can be a bitch...
The Kegworth and transAsia(ATR) accidents involved actually shutting down the good engine followed by an eventual scramble to get it started again. Gpoing fropm memory of the Kegworth report, it appeared that the analysis of the condition of the engines was done quickly by the F/O and accepted by the captain. There is no rush. Just take time and analyze. I suspect that when the engines have been reduced to a lower power setting, it makes it more difficult to identify a partial failure. Perhaps move thrust levers to see reaction on the guages and take your time unless there is a specific reason to be hasty).

It looks like this case is a perfectly good engine that was brought to idle but was still running, and in a position to be immediately used but assumed to be faulty and left at idle. From a procedure point of view, one wonders why they didn't take the time to shut it down if they thought it was faulty. Quite odd.

But on the other hand, seeing as they didn't follow typical procedures and shut down what they thought was a faulty engine, their atypical procedure left them with a big advantage........the ability to use the engine at idle, regardless of whether it was faulty or not. It appears that they thought they had two bad engines. But why would you not attempt to use that engine as things get worse and worse with the GPWS sounding and the altitude and speed decreasing. It would seem that it was assumed that because the engine at idle was in poor shape, it was never considered but one should definitely have in mind that they will take whatever they can get from what is assumed to be a bad engine as it could prevent a crash. Get what you can from both of them in such a situation(and in this case, they would have gotten a bunch of thrust from when they thought they wouldn't get much).

Last edited by punkalouver; 23rd Dec 2022 at 01:52.
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Old 23rd Dec 2022, 05:47
  #297 (permalink)  
 
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Actually, the Kegworth disaster would suggest that changing the flight deck from what the crews are used to might be a bad idea
The Captain had a total of 763 hours on 200, 300, 400 but only 23 of those hours on the 400. Copilot 192 total 300 and 400, 53 of those on 400. Report mentions the reduced conspicuousness of the vibration indicators on the 400 and the fact crews didn't have any simulator time on the 400. Haste in shut down, all not helped by high workload associated with the diversion. Gotchas creep out from everywhere.

Report

https://assets.digital.cabinet-offic...990_G-OBME.pdf

Commentary on panel layout

https://assets.digital.cabinet-offic...BME_Append.pdf
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Old 24th Dec 2022, 21:47
  #298 (permalink)  
 
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Quotes(in black) from a Flight International article based on NTSB information.....

"The first officer, who was flying, replied “number two” – an apparent reference to the right-hand powerplant – and the captain also said, “number two”.

According to the quote above, the captain repeated what the F/O said(unknown if he based his reply on separate analysis). Then according to the quote below, the copilot changed his mind and the captain did as well(unknown what further assessment was made by the captain before he changed his mind).

"According to the transcript, the captain asked the first officer to “read the gauges” to determine which “has the EGT” – the exhaust gas temperature – to which the first officer replied: “It looks like the number one.”The captain then responded, “Number one is gone?”, and the first officer responded: “[It’s] gone, yep…so we have number two.”

“So we have number two, OK,” the captain then remarked."

The captain made this statement to the inquiry.....

"The captain told the inquiry that he thought the left-hand engine had the problem, at first, before changing his mind – based on the aircraft’s yaw and roll motion – and telling the first officer that he thought the right-hand engine was the one affected.

But during his testimony the captain referred to the first officer’s having told him that the number one engine, the left-hand powerplant, had failed.

The captain told investigators that the first officer, which whom he had flown several times, “never makes a mistake”, adding: “If [he] says number one is gone, then number one is gone.”

A bit of a conflict in statements but quite the trusting captain. Based on the CVR recording, it seems quite possible that the captain did change his mind based on what the F/O said, instead of analyzing the problem.


This reminds me of the Kegworth accident when it comes to failed engine identification. To quote the report.....

"The first officer also said that he monitored the engine instruments and, when asked by the commander which engine was causing the trouble, he said 'IT'S THE LE ... IT'S THE RIGHT ONE.', to which the commander responded by saying 'OKAY, THROTTLE IT BACK'."

Once again, no detail on what analysis that captain did, but it does give one the feeling that he may have relied on what the copilot said instead of confirming himself(captain was flying). One really should take extra time to identify a partial engine failure, if time permits. the consequences of a mis-identification can be catastrophic. In addition, a partial failure may not be obvious after thrust has been reduced.

Last edited by punkalouver; 24th Dec 2022 at 23:41.
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Old 25th Dec 2022, 02:23
  #299 (permalink)  

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My type has a TL indication, commanded EPR target if you will. Already rated a few years when I copied someone's technique to visually observe how that doughnut moves - on the dead engine - as I pull the TL back to idle.

And later added an extra eyeflow myself, to confirm what the remaining good engine is doing AFTER closing the TL, i.e. BEFORE taking the next step of selecting the master switch/fuel shutoff. Which is a pretty universal tool technique.

Once this became a habit, I get stunned at how little is being actually checked by colleagues in the SIM who do the same as I used to (admittedly we always got it correct).

Last edited by FlightDetent; 25th Dec 2022 at 13:37.
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Old 25th Dec 2022, 07:06
  #300 (permalink)  
 
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Originally Posted by punkalouver
Quotes(in black) from a Flight International article based on NTSB information.....

"The first officer, who was flying, replied “number two” – an apparent reference to the right-hand powerplant – and the captain also said, “number two”.

According to the quote above, the captain repeated what the F/O said(unknown if he based his reply on separate analysis). Then according to the quote below, the copilot changed his mind and the captain did as well(unknown what further assessment was made by the captain before he changed his mind).
SNAP......
Once again, no detail on what analysis that captain did, but it does give one the feeling that he may have relied on what the copilot said instead of confirming himself(captain was flying). One really should take extra time to identify a partial engine failure, if time permits. the consequences of a mis-identification can be catastrophic. In addition, a partial failure may not be obvious after thrust has been reduced.
Or so to say, tick the QA items, without checking ? Where did we see that before ? Boeing ('s production) ?

I think, the more the "actions" are physical, the more people are inclined to take things for granted and leave out the "logic" items, since that does require a change in mental attention, from the steam gauges and levers attention, over to check-list booklets. With the whole being more "push-button" oriented, it needs mental attention to what the meaning of the buttons is, and the drivers are already in that mental state to "think" what they are doing.
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