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-   -   King Air down at Essendon? (https://www.pprune.org/pacific-general-aviation-questions/591237-king-air-down-essendon.html)

Horatio Leafblower 10th Sep 2018 13:20

I have heard that the rudder trim was found set hard left, FWIW.

Lead Balloon 10th Sep 2018 14:04

I’ve heard the Giant Flying Spaghetti Monster’s Noodly Appendage was responsible for causing a loss of power in one engine. (Which kinda shows why a timely report by an expert investigatory body can be useful.)

junior.VH-LFA 10th Sep 2018 14:19


Originally Posted by bolthead (Post 10245697)
I'm hearing rumours suggesting that diligently checking the trims before takeoff would be a very good idea.

You mean like how it say's in the Before Takeoff Checklist?

It would explain why the aircraft ended up taking out runway lights before even making it airborne. Doesn't explain why there wasn't an abort.

mattyj 11th Sep 2018 00:25

Some pilots are want to wind in a lot of rudder trim in the event of an asymmetric event..so what if the trim was fully applied?

junior.VH-LFA 11th Sep 2018 00:28


Originally Posted by mattyj (Post 10246147)
Some pilots are want to wind in a lot of rudder trim in the event of an asymmetric event..so what if the trim was fully applied?

" That examination found that the cores of both engines were rotating and that there was no evidence of pre-impact failure of either engine’s internal components."

Old Akro 11th Sep 2018 01:07


" That examination found that the cores of both engines were rotating and that there was no evidence of pre-impact failure of either engine’s internal components."
Junior. Rotating and producing power are 2 different things.

Connedrod 11th Sep 2018 02:31

It be easy to see if if the wife’s were making pwr just by the b to c flange position. From what I have heard they were making pwr.

Lookleft 13th Sep 2018 04:23


I have heard that the rudder trim was found set hard left, FWIW.
There was a 310 out of Tamworth in 2005 that got airborne and rolled over on its back with an obvious outcome. It took the ATSB a while to work that out but eventually they come to the conclusion that it had come out of the hangar with the rudder trim set full left. The pilot was to ferry it to Scone and was in a rush so missed the trim part of the checklist. If the trim on the Kingair was full left then it would go a long way to explain the flight path. If the pilot thought he had suffered an engine failure but the engines were producing power then there is too little time available to do any trouble shooting.

Lead Balloon 13th Sep 2018 04:44


It took the ATSB a while to work that out.
Date of accident: 7 March 2005.

Date of Report: 21 June 2007.

Over 2 years seems about par for the ATSB course.

Lookleft 13th Sep 2018 08:15

The problem for an investigation, if it is an incorrect trim setting, is that often the evidence can be destroyed in the crash.

Captain Nomad 14th Sep 2018 05:18

Lookleft, the Tamworth accident has stayed with me. I knew the pilot and was one of the witnesses interviewed by the ATSB in that report.

While it is a great report I have always had lingering doubts about the findings which have not always sat well with me. There is an element to accidents where we may not always conclusively know everything after the event.

For example: "During the on-site examination of the wreckage, investigators located a number of tools including a damaged hand tool (Figure 6) that would not normally be expected to be carried on the aircraft."

...and: "The location of the bent hand tool in the wreckage raised the possibility that it may have contributed to the flight control difficulty. Despite the tool being found in the wreckage, it was not possible to establish whether it was in an internal section of the aircraft that contained part of a primary flight control system or when it had been introduced.
The bending damage to the tool was found to be consistent with severe impact and breakup forces and there was no evidence that the tool had interfered pre-impact with a control system. Such evidence, however, may not have been detectable post-accident."

The report investigates a number of possible probable causes, control interference, trim runaway, autopilot problem, and trim settings. In this case they concluded the report with what they believed to be a 'most probable' cause although other factors certainly cannot be ruled out:

"The limited evidence did not allow the investigation to be certain about the existence of abnormal rudder and/or aileron trim settings during the flight. However, in the absence of any other likely factor and with supporting evidence, the investigation considered that the pilot probably took off with abnormal rudder and/or aileron trim settings and with increasing airspeed, was unable to maintain control."

Flying over the smoking hole in the ground, attending the funeral of a talented young man with his devastated young bride dressed in black, grieving with the family over a life cut all too short (he wasn't even supposed to have been flying that day) stays in ones memory... RIP Jason C.

Be ever vigilant out there folks...

Lookleft 14th Sep 2018 05:32

I know what you felt and continue to feel about losing a colleague and friend CN. My first attendance at a pilot's funeral was at age 24 and that is a long time ago. There were quite a few after that. Never gets easy. No report is easy to read when it involves someone you know.

Horatio Leafblower 14th Sep 2018 12:47


... I have always had lingering doubts about the findings which have not always sat well with me.
We have probably met, Nomad. I too knew the young bloke and there are still whispers around Tamworth about the 'real' cause.

wishiwasupthere 22nd Sep 2018 06:00

ATSB website lists the report release date as 24 Sep 2018 (this coming Monday)?

Grogmonster 22nd Sep 2018 06:51

I have also heard the rumours that the rudder trim was found fully hard over to the left. It may have been but who knows if it was that way prior to impact. I very much doubt the rudder trim theory. From my experience I would suspect that the aircraft is almost impossible to keep straight and would very quickly veer off the runway resulting in an abort. I have experienced the friction nut scenario in the aircraft during an early morning take off and it definitely gets your attention. I have run the Essendon loose friction nut scenario in the Sim and ended up very close to the same spot as old mate.

Groggy

OZBUSDRIVER 24th Sep 2018 00:09

ATSB is handing down its report...not good for pic. Rudder trim and takeoff weight.

outnabout 24th Sep 2018 00:58

Exceeded MTOW??

With 5 POB on a day trip (so I would suspect limited luggage)....it begs the question - what the hell else was on board??

Lead Balloon 24th Sep 2018 01:10

I owe ATSB an apology. They brought this one in before the two year mark.

Pearly White 24th Sep 2018 01:19


Originally Posted by OZBUSDRIVER (Post 10256611)
ATSB is handing down its report...not good for pic. Rudder trim and takeoff weight.

Oh dear. No doubt the regulator will emerge spotless and the people blamed will all be unable to answer for themselves.

Airbubba 24th Sep 2018 01:27

Synopsis of the ATSB report:


What happened

On the morning of 21 February 2017, the pilot of a Beechcraft B200 King Air aircraft, registered VH-ZCR was conducting a charter passenger flight from Essendon Airport, Victoria to King Island, Tasmania with four passengers on board.

The aircraft’s take-off roll was longer than expected and a yaw to the left was observed after rotation. The aircraft’s track began diverging to the left of the runway centreline before rotation and the divergence increased as the flight progressed. The aircraft entered a shallow climb followed by a substantial left sideslip with minimal roll. The aircraft then began to descend and the pilot transmitted a Mayday call. The aircraft subsequently collided with a building in the Bulla Road Precinct Retail Outlet Centre of Essendon Airport.

The aircraft was destroyed by the impact and post-impact fire, and all on board were fatally injured. The building was severely damaged and two people on the ground received minor injuries.

What the ATSB found

The ATSB found that the pilot did not detect that the aircraft’s rudder trim was in the full nose-left position prior to take-off. The position of the rudder trim resulted in a loss of directional control and had a significant impact on the aircraft’s climb performance in the latter part of the flight.

At the time of the accident, the operator did not have an appropriate flight check system in place for VH-ZCR. Although this did not contribute to this accident, it increased the risk of incorrect checklists being used, incorrect application of the aircraft's checklists, and checks related to supplemental equipment not being performed.

The aircraft’s cockpit voice recorder did not record the accident flight due to a tripped ‘impact switch’, which was not reset prior to the accident flight. This deprived the investigation of potentially valuable recorded information.

The ATSB determined that the aircraft was operated above its maximum take-off weight on the accident flight. This was not considered to have influenced the accident.

The ATSB also found that the presence of the building struck by the aircraft did not increase the severity of the consequences of this accident. In the absence of that building, the aircraft’s flight path would probably have resulted in an uncontrolled collision with a busy freeway, with the potential for increased ground casualties.

Although not contributing to this accident, the ATSB identified that two other buildings within the retail precinct exceeded the airport’s obstacle limitation surfaces. While those exeedances had been approved by the Civil Aviation Safety Authority, the ATSB identified several issues relating to the building approval process for the precinct.

What's been done as a result

It is beyond the scope of this investigation to consider in detail the issues identified with the Bulla Road Precinct building approval processes. These issues will be addressed in the current ATSB Safety Issues investigation The approval process for the Bulla Road Precinct Retail Outlet Centre AI-2018-010.

Safety message

Cockpit checklists are an essential tool for overcoming limitations with pilot memory, and ensuring that action items are completed in sequence and without omission. The improper or non-use of checklists has been cited as a factor in some aircraft accidents. Research has shown that this may occur for varying reasons and that experienced pilots are not immune to checklist errors. This accident highlights the critical importance of appropriately actioning and completing checklists.

This accident also emphasises the importance of having flight check systems in place that are applicable to specific aircraft in their current modification status. In addition, it emphasises:
  • the value of cockpit voice recorders
  • the significance of ensuring aircraft weight and balance limitations are not exceeded
  • the challenges associated with decision-making in critical stages of a flight such as the take-off ground roll.



https://www.atsb.gov.au/publications/investigation_reports/2017/aair/ao-2017-024/

Lead Balloon 24th Sep 2018 01:34

I do not understand how the bolded bit is supportable on the facts:

The ATSB also found that the presence of the building struck by the aircraft did not increase the severity of the consequences of this accident. In the absence of that building, the aircraft’s flight path would probably have resulted in an uncontrolled collision with a busy freeway, with the potential for increased ground casualties.
Isn’t the building located on the aerodrome side of the “busy freeway”?

Flingwing47 24th Sep 2018 01:41

I didn't see all the ATSB presentation....thanks ABC for switching away.
Was the question asked as to why the rudder trim was in the full left position?
Had the aircraft had any recent maintenance done that would have involved the rudder trim mechanism ?

Old Akro 24th Sep 2018 01:52

If it was just rudder trim, why did the report take nearly 2 years?

From my initial scan of the report:

As i understand it, the PIC was the last person to fly the aircraft. So, who moved the trim?

The report infers that the pilot did not undertake a proper pre-flight, but despite CCTV footage is unable to provide any factual evidence - only speculation.

It notes that the preflight checks have 5 separate checks of the rudder trim, but has nothing other than speculation that says these were not conducted.

Examination of the wreckage clearly shows full LH rudder trim, but the report is mute on when or how it got that way.

Old Akro 24th Sep 2018 03:09


Originally Posted by GAforlife (Post 10256668)
Too much fuel?

ATSB say that based on ITS OWN estimation that the aircraft was 240kg over weight out of a total of 5670kg - or 4%. It also says that the CofG limits were within the fore / aft limits. this equates to 48 USG of the fuel capacity of 549 USG. I'd say that the ATSB is being too cute and that the 240kg it alleges that the aircraft was overweight was within the area of uncertainty of their estimation.

Old Akro 24th Sep 2018 03:17

I think the B200 is an FAR 25 type certificate? Does anyone know if the type certificate requires demonstration that the aircraft is controllable with full rudder trim?

When the Partenavia that crashed at Essendon in the 1970's and it was found that the aircraft was not controllable at full elevator trim, an emergency AD was issued requiring the elevator trim to be limited. If the B200 is not controllable with full rudder trim, should there be a recommendation from the ATSB about an AD for B200 aircraft to limit rudder trim?

Car RAMROD 24th Sep 2018 03:33

Akro, it's Part 23. Raisebeck does have a Part 25 supplement though.

3100lbs (full mains and 400ltrs in the aux tanks) for a flight to King Island and back? That's a heck of a lot of fuel! With 5 on board and gear, that could well be pushing limits depending on the BEW of the aircraft. Most would struggle to load 500kg (pilot/pax/bags) with that amount of fuel on board.

As for the stated cause in the report, I'm speechless.

Lead Balloon 24th Sep 2018 03:33

FAR 23 methinks....

Traffic_Is_Er_Was 24th Sep 2018 03:52


Originally Posted by Lead Balloon (Post 10256648)
I do not understand how the bolded bit is supportable on the facts:Isn’t the building located on the aerodrome side of the “busy freeway”?

It hit the edge of the building, and ended up in the rear car park. Beyond that car park in the direction of flight is the freeway.

Squawk7700 24th Sep 2018 03:55

You’d have to assume it’s far more convenient to leave with a full fuel load rather than pay Tasmanian prices for a refill.

Theres no point suggesting who / what is responsible for winding it to the left because it is irrelevant if it was missed before takeoff. All that would do is incriminate additional parties and not affect the outcome other than from a possible litigation perspective, despite that being a hard ask.

Can anyone think of an operational reason as to why it would be so far across, perhaps from a previous flight?


Does anyone know if the type certificate requires demonstration that the aircraft is controllable with full rudder trim?
I guess it’s a moot point if it was over weight. All bets would be off on certification requirements.


WetCompass 24th Sep 2018 04:09


The ATSB also found that the presence of the building struck by the aircraft did not increase the severity of the consequences of this accident. In the absence of that building, the aircraft’s flight path would probably have resulted in an uncontrolled collision with a busy freeway, with the potential for increased ground casualties

So if we follow that reasoning should there be a recommendation to line all airports with buildings to protect the roads?

Pearly White 24th Sep 2018 04:17


Originally Posted by GAforlife (Post 10256668)
Too much fuel?

Weren't the Americans on a golfing holiday and planning to play a game at King Island? So they would have had golf clubs, which probably weigh 10-15kg a bag, maybe more. Don't know, I don't play. And given that fuel is likely quite expensive on the island, the fuel plan would have involved tankering. And what were they carrying as an alternate, DPO? Another 250km away...

outnabout 24th Sep 2018 04:23

Thanks for the additional info.

I have to say, I am extremely surprised that full mains, 400 litres in the auxers, five adults, and possibly four golf bags, puts the aircraft at an estimated 240kgs overweight.

I have no experience at all on the B200, but I assumed, naively, that they would have more payload than that.

Old Akro 24th Sep 2018 04:26

The ATSB report says that the B200 is controllable with full left trim up to 140 KTAS (p46)
The ground speed data shows that the aircraft took off at 11 kt GS and peaked at approx 116 kt before decaying to approx 108 kts at impact (p28)
actual MET data recorded at 1 sec intervals shows the wind at 322 deg magnetic at 4-5 kts for a tailwind component of approx 4 kts
Therefore TAS of the aircraft is (approx) 107 kt (rotation) 112 kt (initial climb) 104 kt (impact).

So... why was the pilot not able to maintain directional control? The ATSB flight simulator exercise shows that at these speeds directional control could be maintained.

Also, why was the aircraft not CLIMBING? If the engines were producing full power, it should have either been diving (increasing airspeed) or climbing. Yet, its airspeed was decaying and it was not climbing.

the ATSB explanation that the cause was sideslip is flawed. The flight simulator testing (p46) was " in order to determine the effects of full left rudder trim on take-off and climb performance" and yet, the ATSB presents no data on take-off or climb performance from the simulator tests and goes on to say " "it was not possible to quantify the effects on ZCR without flight testing or complex engineering modelling. Both of these options was outside the scope of investigation...". This is the very core of the issue that the ATSB conclude, but they say its outside the scope of the investigation????? Really??

The ATSB has labelled the cause as full left rudder trim, yet has not put forward an explanation how it occurred, or how a pilot with 2400 hours on B200 all of a sudden forgot. Nor has the ATSB made any real attempt to prove its theory that the rudder trim led to yaw which led to lack of climb performance. The simulator work that the ATSB commissioned demonstrated that the aircraft could maintain directional control by the pilot at the airspeeds recorded by VH-ZCR. So why didn't a very experienced B200 pilot not push harder on the rudder, keep the aircraft straight and fly away?

Capt Fathom 24th Sep 2018 04:26


You’d have to assume it’s far more convenient to leave with a full fuel load rather than pay Tasmanian prices for a refill.
It's 40 mins each way, so would hardly need a refill. Unless the plan was to fly somewhere else before returning to Essendon?

While the report tells us what caused the accident, there are certainly many unanswered questions.

Car RAMROD 24th Sep 2018 04:31

Squawk, no need to take full fuel just to avoid paying Tassy prices. Take what you need and then some, no problem. But I would say, on face value, without any extenuating circumstances, that 3100lbs is excessive for that kind of trip- especially in the commercial world (unless you disregard W&B, which some do). 3100 isn't full fuel anyway.

I'd quite comfortably do that trip, with no weather requirements, with 2100lbs. That's a bit over 30 mins margin on top of 30 fixed back at Essendon. Not exactly scary. Or to make life easy, full mains 2400lbs- gives me another 40mins margin back at EN plus no worries with the payload. Plenty of alternate and divert options.
And if you are likely to need fuel in Tas, build it into the charter cost!
Note- I'm basing the above two paragraphs on the assumption that it was just an EN-KI-EN trip.

Hell, you can take a B200 most of the way across the country with 3100lbs!


In relation to the rudder trim setting- the only real reasons why it would be there are- single engine flight (you still don't need full deflection); maintenance; or checking the full travel on pre-flight and forgetting to set it back to neutral afterwards.


outnabout- probably the only thing I don't like about the B200 is its payload when you stuck heaps of fuel in there. That's where the 350 is better. You'll find a lot of B200s are around the 3700-3800kg range empty. Varies a lot though with interiors, props (3 or 4 blade), other airframe and performance mods, landing gear, avionics fitouts (going from a standard avionics panel to a full glass can save about 60kg) etc etc.
VIP/executive type interiors (which ZCR had) are typically heavier than the "commuter" type configurations. The only one I flew with VIP config was about 100kg heavier, and that was just in the seats!

Old Akro 24th Sep 2018 04:34


I guess it’s a moot point if it was over weight. All bets would be off on certification requirements
It was 4% overweight by the ATSB's estimation - for which they have presented no details.

the PIC was reasonably light. Lets call the passengers 100 kg ea with 30 kg of bags each. This should still leave over 1300kg for fuel. Google tells me a bit over 100 gph in the cruise = about 320kg/hr = 4 hours range. Even with the new CASA fuel reserves that seems a lot for King Is & back.

Victa Bravo 24th Sep 2018 04:48


Originally Posted by Car RAMROD (Post 10256698)

In relation to the rudder trim setting - the only real reasons why it would be there are- single engine flight (you still don't need full deflection); maintenance; or checking the full travel on pre-flight and forgetting to set it back to neutral afterwards.

Bingo. Checked the full travel of the trim tab in the pre flight combined with Old mate's propensity to wing the checklists and she's heading for the shops....

mostlytossas 24th Sep 2018 05:16

Well so much for the PPrune experts. having just reviewed the topic from start to finish the following reasons for the crash were. Engine failure and/ or both, water in hull, Torque set too low, throttle friction locks, and even control seat collapsed/went backwards. No one picked the rudder trim set right over. Dick Smith in a way came closest when in April stated this would never had happened if the pilot was grounded after he had an incident at Mt Hotham some time previous see post 716.( My guess Dick had some inside info on the investigation this time). So sadly it appears the pilot in question did not use a check list, never been in a sim and apparently stated he didn't need to. His carefree attitude finally caught up with him and sadly he took his passengers with him.
Lesson for all of us.

TWT 24th Sep 2018 05:25


sadly it appears the pilot in question did not use a check list
Some of the people he flew with said he did use a checklist, some said he didn't. It could not be determined if he used a checklist on this flight.

holdingagain 24th Sep 2018 05:43

Maybe x 2

the aircraft was refueled for a previous booking which was cancelled leaving a fuel excess for this flight

he was mid way through his trim preflight check, answered his mobile and missed returning the trims to the take off possition



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