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Alaska Airlines 737-900 MAX loses a door in-flight out of PDX

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Alaska Airlines 737-900 MAX loses a door in-flight out of PDX

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Old 8th Jan 2024, 12:24
  #381 (permalink)  
 
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Originally Posted by C2H5OH
That's what I thought when I first saw that axial bore. I further thought, that the bolt may slide into that fitting by installing a tool and pulling towards the center of the plug. However this is not compatible with the infos given by the 737 tech channel.
As said before this stub of the roller pin is rather short. I wonder if it is still blocked if wrong diameter locking bolts are used.
The roller pin cannot be any longer than the opening in the bottom of the guide allows for. Looking at the RH image, there is a significant bit of the roller pin inside the guide and the locking pin is centralised relative to the width of the opening at the bottom of the guide. I posed a question earlier on whether the roller pin could perhaps have moved past the locking pins with a bit of flexibility, but I cannot see that happening (based on these images), especially as it would mean both pins being too short and both sills moving outwards (in opposite direction).

Just a guess, but the hole in the centre of the roller pin may be for adjustment of this pin. It probably does not allow a bolt to be fitted in there. The suggestion earlier on of using this hole to lock the assembly would not allow for the same provisions for locking the bolt in place, would be more difficult to inspect and would put extra stresses on the roller pin mounting. The locking pin as it is used by Boeing here is a much simpler option as it prevents movement of the pin relative to the guide by blocking this guide, which is what is needed in this case.
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Old 8th Jan 2024, 12:30
  #382 (permalink)  
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fdr's post of historic incident with Boeing and their sub contractors. Indeed, the latter was caught with their pants down on a Swat style inspection. The specifications for those rings was to an accuracy of 3,000 th of an inch., but were being hand honed with what looked like sanding blocks. Some aircraft had the rings so tight they were hammered into place and it seems, marked with colour to show where. The treatment of those women left me breathless, though I don't know why in the poisonous culture Boeing had allowed to flourish.

Last time that occurred, the Renton QA Staff visited the supplier to Boeing who was doing the ring frames for the NG, and noted that the frames which the production approvals had been based on CAM milling, were being done by hand, over an unapproved homemade jig. The supplier had stated the components were CAM fabricated, and they didn't own a CAM unit. Upshot, Boeing sacked the QA inspectors, and Boeing actually won in court against wrongful dismissal action by the inspectors. The FAA did... nothing. The bogus parts are still flying around today.
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Old 8th Jan 2024, 12:48
  #383 (permalink)  
 
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Originally Posted by Phantom4
MechEngr,Would the position of this door be subjected to large torsional stresses??
My initial thought was that the door was made of unsuitable materials, particularly the fingers, or that an operation left a gouge to raise stresses; that thought has been put aside.

The rigidity of tubular fuselages limits torsion deformation. Without deformation there isn't much stress on the door. The main stress is from the pressure load which puts bending loads on the fingers, but if they had failed the guide rollers would likely have been torn loose and they are still present.
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Old 8th Jan 2024, 13:05
  #384 (permalink)  
 
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Originally Posted by JamaicaJoe
A couple comments:
1) Can we all agree that the missing part of the plane is a "door" that replaces an emergency exit "door, That it is NOT a "plug"?, it is not designed as a "plug", does not function as a "plug" under pressurization of the hull. In fact, it performs exactly the opposite. The outward forces work to stress the door against its retainers not the frame in any intrinsic or hermetic manner..

2) The missing door is fitted with a larger window than the emergency door it replaces. It seems from photos that there is less cross bracing in that design. However I am not jumping to conclusions that the door failed. It is more likely that the low altitude and missing bolts conspired to eject this door (not a plug).
No, a door is a door. It can be opened and closed at will.
A door on an aircraft can be a plug type door where cabin pressure forces the door to the closed position.
The item that detached from this aircraft was not a door, it was a panel designed to fill an unused opening in the fuselage.
When owners of older 707/727/737 aircraft choose to no longer use the eyebrow windows in the cockpit, they don't replace them with doors, they replace them with plugs.
Same when passenger aircraft are converted for cargo use, the cabin windows are replaced with plugs. Not doors.
Photos have been posted in this thread showing the inside of both the doors and the plugs that can fill this opening in the fuselage. They are not the same.
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Old 8th Jan 2024, 13:15
  #385 (permalink)  
 
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Originally Posted by JamaicaJoe
SWAG Theories

1) The popular one. Rigging was incorrect, one or more bolts left out that would have prevented the door (not a PLUG) to move from its fully engaged position.

2) a) Photos of one guide pin on the accident plane appear to show a very short length of the guide pin/roller. Its length significantly less than its diameter. b) The dummy door (not a PLUG) differs from an Emergency Exit Door (not a PLUG) in a significant way. The cross bracing is removed to accommodate a larger window. Could the combination of the panel being weaker at that point have allowed the door (not a PLUG) to bow outward and dislodged the upper portion of the door from the guide pins/rollers? The four rigging bolts would do little to retain the door at this point.
Please contact the FAA and show them the error of their ways and have them correct the use of the word "plug" in the Emergency Airworthiness Directive.
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Old 8th Jan 2024, 13:15
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NTSB B-Roll - Alaska Airlines Flight 1282 Boeing 737-9 MAX



Check out 2:12 - the right side is being examined and light is coming through. Either the NTSB opened the right side for inspection, or the right side was also not secured.
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Old 8th Jan 2024, 13:24
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Originally Posted by fotoguzzi
Hello, I have read that this panel can be opened from outside. That must be wrong, correct?

To my comprehension, the interior paneling would need to be removed and fasteners removed from the panel before the "drop down" mechanism could be deployed.
Possibly some confusion with the emergency exit that can be fitted in lieu of the door plug and that can, like any E/E, be opened from both inside and outside.
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Old 8th Jan 2024, 13:32
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Originally Posted by chrismc1977

From the images there would appear to be 6 bolts per side installed at manufacture which additionally hold the plug in position vertically & horizontally. These shouldn’t take any of the pressurisation loads however.
That is incorrect, they are just contact points not bolted together.
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Old 8th Jan 2024, 13:41
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Originally Posted by WHBM
Even more significant was the air rush sucked the emergency SOP checklist out of the flight deck. Which presumably contained the CVR switch off command. The crew had to do it all from memory instead.

One day the CVR industry will come up with an ever so simple way to avoid this overwriting. Goodness knows how often it has occurred in incidents in the past. I know the requirement is to maintain the last 2 hours, but that didn't extend to any instruction to start overwriting at 2 hours and 1 minute.
With just about every new aircraft having internet access on board you would think it would be very easy to stream the entire aircraft life history to the cloud (no pun intended) as a back up to on board orange boxes.
Or relegate the on board boxes to the back up role.
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Old 8th Jan 2024, 13:47
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Originally Posted by tdracer
Before you all get too wrapped up in your anti-Boeing crusade, you might want to consider this little inconvenient fact: The fuselage isn't built by Boeing - all 737 fuselages are assembled in Wichita by Spirit AeroSystems. The fuselages are shipped to Renton by rail as basically complete structures with the plug (or door) already installed. Assuming that this was an assembly issue (as seems likely based on the lack of associated damage from the departed plug, as well as the AD'ed inspection), the blame should fall squarely on Spriit, not Boeing.
While Spirit was "Boeing Wichita" at one time, that hasn't been the case for nearly 20 years (Boeing sold them in 2005) and it has operated as an independent subcontractor since. Spirit is also a major supplier to Airbus.
While an alert inspector at Boeing might have picked up on missing fasteners, given that fuselage portion arrives as a compete, approved assembly, it is very unlikely that there is any task at Boeing Renton to verify that the appropriate fasteners are installed on that door plug.
Unfortunately, QA at Spirit has been an on-going issue for some time - especially with the 737 fuselages (the often-mentioned issue with the miss-drilled aft bulkhead holes also traces back to Spirit.
Interestingly, there was an article in the Seattle Times recently regarding Boeing and Spirit re-negotiating the contract for the 737 fuselages to include improved quality and QA inspections (presumably with an increase in price to Boeing, although I don't think the article specifically said that).

While I doubt it's feasible at this point for Boeing to bring in a new subcontractor for the 737 fuselage, I think Spirit badly needs to step up their game if they expect to receive any future new business (Boeing, Airbus, or anyone else). No airframer wants to be associated with the sort of liability (not to mention bad press) that the recent Spirit screwups have caused Boeing.
"On a Wing and a Prayer" by Al Jazeera covered exactly this issue.
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Old 8th Jan 2024, 13:49
  #391 (permalink)  
 
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Originally Posted by WHBM
Even more significant was the air rush sucked the emergency SOP checklist out of the flight deck. Which presumably contained the CVR switch off command. The crew had to do it all from memory instead.

One day the CVR industry will come up with an ever so simple way to avoid this overwriting. Goodness knows how often it has occurred in incidents in the past. I know the requirement is to maintain the last 2 hours, but that didn't extend to any instruction to start overwriting at 2 hours and 1 minute.
With just about every new aircraft having internet access on board you would think it would be very easy to stream the entire aircraft life history to the cloud (no pun intended) as a back up to on board orange boxes.
Or relegate the on board boxes to the back up role.

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Old 8th Jan 2024, 13:50
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Originally Posted by Peter Fanelli
With just about every new aircraft having internet access on board you would think it would be very easy to stream the entire aircraft life history to the cloud (no pun intended) as a back up to on board orange boxes.
Or relegate the on board boxes to the back up role.
The advance of technology and reduction in cost makes it VERY hard to understand why on-board systems are limited to 2 hours voice - investment in aircraft and piloting tech seems to have left this subsystem behind.

Transmission to cloud-based storage is currently not sufficiently reliable for real time use, but burst transmission for (infinite) archive would be achievable at what OUGHT to be only a minor cost per hour.
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Old 8th Jan 2024, 13:55
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Something is prompting the NTSB boss to photograph it. I imagine the denuded view will be somewhat interesting.

Not the boss, the plug!
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Old 8th Jan 2024, 14:06
  #394 (permalink)  
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Originally Posted by Loose rivets
Something is prompting the NTSB boss to photograph it. I imagine the denuded view will be somewhat interesting.

Not the boss, the plug!
I don't see that you can conclude the door/plug is not secured from the video. It could be that the decor panel and window surround has separated from the window allowing light to enter between the inside of the window and window surround. Why that might have happened is another matter. It might just be a result of the loss of pressurisation.
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Old 8th Jan 2024, 14:10
  #395 (permalink)  
 
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Unconfirmed reports that the newly-discovered door plug has one of the two guide rollers jammed in the guide. Given that they are part of the aircraft structure and not the door, if true it would imply that it had sheared off.

That would be an interesting failure mode. Given that the photos appear to show the aft roller still in situ in the doorframe, it would have to be the forward one. With no guide roller engaged in the door, the presence or absence of the locking bolt would be irrelevant and it may have allowed at least the forward edge of the door to creep past the stops.
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Old 8th Jan 2024, 14:11
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Originally Posted by oscarbravo2
The stop pads are installed the wrong way round, for use as operating door the pins in the stop pads should face out and for inactive door using a door plug they should face in. Just another assembly mistake :-)
You didn't take up my earlier suggestion to call the NTSB with your findings, then ?
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Old 8th Jan 2024, 14:39
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Originally Posted by Maninthebar
The advance of technology and reduction in cost makes it VERY hard to understand why on-board systems are limited to 2 hours voice - investment in aircraft and piloting tech seems to have left this subsystem behind.

Transmission to cloud-based storage is currently not sufficiently reliable for real time use, but burst transmission for (infinite) archive would be achievable at what OUGHT to be only a minor cost per hour.
ISTR that, back in the day, there was a confidentiality issue with getting crews to initially accept the presence of CVRs (the "spy in the cockpit"; c.f. commercial automotive duty-time recorders), as they would be recording not only pertinent exchanges of information, but also the private conversations of the crew; conversations that might not always reflect their views on colleagues, Corporate policy and so forth in the best light. Hence, they were only acceptable to pilots' unions on the basis that the recording remained on the aircraft, under the the control of its crew, until such time as the aircraft safely reached its destination, when the "and-gate" of weight-on-ground, and engine shutdown, enables operation of the ERASE button in order to delete the record so that "what happened in Vegas stayed in Vegas". Beaming the conversations, live, to a cloud might encounter similar resistance.

I take your point about the 2-hour thing but, at some point, it still needs someone to pull the CB. Think 24 hours is going to cut it?
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Old 8th Jan 2024, 14:45
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Originally Posted by aeromech3
Even if the 4 locking bolts (with their slotted nuts and cotter pins/split pins) were missing, the lower hinge arms which are still attached to the floor bracket, have a double lock nut arrangement on the shaft end and large washer, allowing the semi plug to rise and hinge outwards, spring assist, as it is apparently designed to do; the exterior fuselage does not appear to have any buffet damage from the plug assembly which indicates to be at least that either the washer was not large enough to hold on the bracket structure and the shaft just pulled through; Or the double lock nuts and washer was not present. Accepted the lanyards are unlikely to offer little resistance to the cabin pressure acting on the large plug surface.
I do not have a good definition screen to zero in on the hinge fittings on the outside to see if there is just thread or nuts present, anyone?
The same thought crossed my mind as well.
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Old 8th Jan 2024, 15:12
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Originally Posted by DaveReidUK
Unconfirmed reports that the newly-discovered door plug has one of the two guide rollers jammed in the guide. Given that they are part of the aircraft structure and not the door, if true it would imply that it had sheared off.

That would be an interesting failure mode. Given that the photos appear to show the aft roller still in situ in the doorframe, it would have to be the forward one. With no guide roller engaged in the door, the presence or absence of the locking bolt would be irrelevant and it may have allowed at least the forward edge of the door to creep past the stops.
The photos on the first page of this thread show both left and right rollers in place in the frame, exactly where they should be.
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Old 8th Jan 2024, 15:28
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Originally Posted by roger4
The photos on the first page of this thread show both left and right rollers in place in the frame, exactly where they should be.
Yes, it does seem to be present although partially obscured by insulation.

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