A20N Engine Start
Thread Starter
Joined: Nov 2004
Posts: 69
Likes: 0
From: EGCC
A20N Engine Start
The A320NEO seems to take an age between pushback and engine startup to request for taxi. Would a more learned subscriber venture the reason(s) why? After push and start the other day, we waited for the 'request taxi' call and an inbound to the ramp had to hold short waiting for the outbound. The flight deck commented on R/T "yes, we're in the NEO; it takes forever..." - what's different about the NEO that makes for a longer startup time? Thanks for enlightening me!


Joined: Sep 2003
Aviation Qualifications: ATPL
Posts: 956
Likes: 68
From: away from home



Joined: Jul 2013
Aviation Qualifications: Non-Aircrew
Posts: 5,678
Likes: 3,341
From: Everett, WA
Exactly. Not familiar with what Pratt does (although I'd be surprised if it's much different), but on the LEAP engine, if residual EGT is above a threshold (which it generally will be if the engine has been shutdown for less than ~six hours), it will motor the engine at a specific N2 speed range (less than max motoring) for about a minute to allow the high rotor to thermally stabilize. Once that's done, it goes ahead and proceeds with the normal start.
GEnx does much the same thing.
Bowed rotor is caused by the differential cooling after shutdown (hot air rises, so the bottom cools quicker than the top...) which will literally result in a small 'bow' in the rotor. Starting the engine with a bowed rotor will cause high vibes and can rub compressor seals resulting in a permanent loss of performance. Worse case it can even cause compressor blades to crack or fracture.
GEnx does much the same thing.
Bowed rotor is caused by the differential cooling after shutdown (hot air rises, so the bottom cools quicker than the top...) which will literally result in a small 'bow' in the rotor. Starting the engine with a bowed rotor will cause high vibes and can rub compressor seals resulting in a permanent loss of performance. Worse case it can even cause compressor blades to crack or fracture.

Joined: Jun 2007
Posts: 3,443
Likes: 39
From: Wanderlust
For fuel efficiency everything about an engine is being made to operate to the limit e. g. Fan diameter to process more air mass, compression increasing core pressure, N1 and higher EGT. So the tolerances are reduced. Older engines had more margins. Some of them also had to motor to bring residual EGT down for start. In PW the separated fan through gearing so it could operate at it's own efficient speed. It allowed them bigger fan and less stages of compression reducing weight.



Joined: Jul 2013
Aviation Qualifications: Non-Aircrew
Posts: 5,678
Likes: 3,341
From: Everett, WA
GE9X on the 777X takes bowed rotor mitigation one step further - there is a small electric motor on the gearbox that uses aircraft power to slowly rotate the core after shutdown at roughly one rotation per minute - that will even out the cooling of the core and prevent the rotor from bowing. It's commonly referred to as the 'rotisserie' for what should be obvious reasons.

Joined: Sep 2016
Posts: 937
Likes: 67
From: USA
GE9X on the 777X takes bowed rotor mitigation one step further - there is a small electric motor on the gearbox that uses aircraft power to slowly rotate the core after shutdown at roughly one rotation per minute - that will even out the cooling of the core and prevent the rotor from bowing. It's commonly referred to as the 'rotisserie' for what should be obvious reasons.

Joined: Jan 2004
Posts: 3,246
Likes: 202
From: Here and there
The IAE engines already had a significant motoring cycle prior to fuel input (about 30 seconds), I don't know if the CFMs had something similar. At least the NEO can cool both engines at the same time, something I gather the B737 MAX does not do.

Joined: Jun 1999
Posts: 2,997
Likes: 35
From: Oztrailia
There’s been a EGT maximum before introducing fuel on big Engines for a long time on the wide bodies I’ve flown. Generally 100c but 150c for some.....Only an issue for turnarounds, especially when there is no wind blowing the Engine around on transit.
.
.
Joined: Dec 2010
Posts: 192
Likes: 0
From: MC80 Home One type Star Cruiser
Interesting info from everyone. Thanks.
Joined: Dec 2010
Posts: 192
Likes: 0
From: MC80 Home One type Star Cruiser




