Make sure you guys are doing your control checks
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Make sure you guys are doing your control checks
TO: All Gulfstream Operators
SUBJECT: General (ATA 05) – Gulfstream IV Aborts Takeoff
On February 7, 2015, a Gulfstream IV operator aborted a takeoff due to failure of the aircraft to rotate. The aircraft was slowed and taxied from the runway, at which time a fire was observed coming from the right brakes. The fire was extinguished and all passengers and crew safely disembarked from the aircraft.
Gulfstream is assisting the regulatory authorities with their investigation. Any fleet action resulting from this event will be communicated accordingly.
If you should have questions or comments regarding this communication, please contact Customer Support at 800-810-GULF (4853) or 912-965-4178, by fax at 912-965-4184, or by electronic mail at [email protected].
Sincerely,
Mitchell A. Choquette
Director, Product Support & Field Service
SUBJECT: General (ATA 05) – Gulfstream IV Aborts Takeoff
On February 7, 2015, a Gulfstream IV operator aborted a takeoff due to failure of the aircraft to rotate. The aircraft was slowed and taxied from the runway, at which time a fire was observed coming from the right brakes. The fire was extinguished and all passengers and crew safely disembarked from the aircraft.
Gulfstream is assisting the regulatory authorities with their investigation. Any fleet action resulting from this event will be communicated accordingly.
If you should have questions or comments regarding this communication, please contact Customer Support at 800-810-GULF (4853) or 912-965-4178, by fax at 912-965-4184, or by electronic mail at [email protected].
Sincerely,
Mitchell A. Choquette
Director, Product Support & Field Service
Well that's a much happier outcome than it was when a G-4 ran off the end at Bedford, MA last year. A similar notice was issued by Gulfstream shortly following that accident too.
westhawk
westhawk
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A follow up from the operator.
All – Attached find the latest MOL from Gulfstream regarding a GIV takeoff abort. Now that this is public, I want to provide some additional information. This was/is a Fair Wind managed GIV aircraft.
The event took place Saturday evening in Eagle, CO (EGE). Crew attempted a takeoff for a part 91 flight and aborted the takeoff at/above Vr due to apparent flight control malfunction. Crew stated that controls felt “unloaded” “mushy” and “unresponsive” and no matter how much they pulled aft on the “resistance free” yoke, the aircraft would not rotate. Crew elected to proceed with a highspeed abort and successfully stopped the aircraft on the 9000 foot runway, exited, stopped on a taxi-way, and requested fire crews due to hot brakes.
Fire trucks responded and about 4 minutes after wheel stop, a fire started on the right main gear brakes deflating tires. Fire was put out and crew and passengers were evacuated.
Aircraft was towed and quarantined in a hangar and NTSB and FAA are now investigating. Fair Wind is party to the ongoing investigation as to the potential causes of this incident.
This is all the information I can share at the moment other than that the crews decisive, correct, and split-second actions resulted in the safe abort and directly preventing the loss of life and property. I am immensely proud of their actions.
As you all know, a few months back, a Gulfstream IV had a similar occurrence in BED that ended in complete loss of life and destruction of the aircraft. We’re glad that all involved are uninjured and harm free.
Alexander H. Beringer
Executive Vice President | Director of Operations
All – Attached find the latest MOL from Gulfstream regarding a GIV takeoff abort. Now that this is public, I want to provide some additional information. This was/is a Fair Wind managed GIV aircraft.
The event took place Saturday evening in Eagle, CO (EGE). Crew attempted a takeoff for a part 91 flight and aborted the takeoff at/above Vr due to apparent flight control malfunction. Crew stated that controls felt “unloaded” “mushy” and “unresponsive” and no matter how much they pulled aft on the “resistance free” yoke, the aircraft would not rotate. Crew elected to proceed with a highspeed abort and successfully stopped the aircraft on the 9000 foot runway, exited, stopped on a taxi-way, and requested fire crews due to hot brakes.
Fire trucks responded and about 4 minutes after wheel stop, a fire started on the right main gear brakes deflating tires. Fire was put out and crew and passengers were evacuated.
Aircraft was towed and quarantined in a hangar and NTSB and FAA are now investigating. Fair Wind is party to the ongoing investigation as to the potential causes of this incident.
This is all the information I can share at the moment other than that the crews decisive, correct, and split-second actions resulted in the safe abort and directly preventing the loss of life and property. I am immensely proud of their actions.
As you all know, a few months back, a Gulfstream IV had a similar occurrence in BED that ended in complete loss of life and destruction of the aircraft. We’re glad that all involved are uninjured and harm free.
Alexander H. Beringer
Executive Vice President | Director of Operations
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Not sure how this could happen unless cables were compromised. There is still a mechanical linkage between the yoke and elevators that is hydraulically assisted not controlled. If you go out to the hangar floor and climb in a dark G-IV you'd find that you can move all the flight controls quite freely using the yoke/pedals, if you were to apply electrical and hydraulic power you would find the controls much stiffer to operate.