Wikiposts
Search
Spectators Balcony (Spotters Corner) If you're not a professional pilot but want to discuss issues about the job, this is the best place to loiter. You won't be moved on by 'security' and there'll be plenty of experts to answer any questions.

TAROM B733-tail strike

Thread Tools
 
Search this Thread
 
Old 4th Apr 2011, 21:43
  #1 (permalink)  
Thread Starter
 
Join Date: Jul 2005
Location: here and there
Posts: 156
Likes: 0
Received 0 Likes on 0 Posts
TAROM B733-tail strike

The plane took off from Otopeni Bucharest (OTP/OMDB) at 9.10 (local time). They had a tail strike which was described by the company as a "minor incident".
They returned to field, landing 09.45 (local time). The plane was grounded for investigations. Pax were shifted to another plane and took off 2 hours later heading to Madrid, their destination.

The plane involved in the incident is YR-BGD (B737-38J, delivered to Tarom to 1994).

no other details available about the incident at this stage.
skytrax is offline  
Old 5th Apr 2011, 10:26
  #2 (permalink)  
 
Join Date: Dec 2004
Location: Where eagles dare
Posts: 31
Likes: 0
Received 0 Likes on 0 Posts
Not trying to be smart here, but how on earth could that be done in a -300
paperdragon is offline  
Old 5th Apr 2011, 11:52
  #3 (permalink)  
 
Join Date: Nov 2003
Location: Amsterdam
Age: 70
Posts: 159
Likes: 0
Received 0 Likes on 0 Posts
Not trying to be smart here, but how on earth could that be done in a -300
Same way as in the -500, get weight/balance wrong, mistrim it, wrong V-speeds and pull up real fast..

Also meteorological phenomenon could be involved
Capt. Inop is offline  
Old 5th Apr 2011, 12:09
  #4 (permalink)  
 
Join Date: Jan 2010
Location: The moon
Posts: 132
Likes: 0
Received 0 Likes on 0 Posts
Or like one captain told me, when he rotated his seat was not fully locked and it slid back while he still held on to the control wheel, resulted in a tailstrike also on a -300
Johnny Tightlips is offline  
Old 5th Apr 2011, 12:56
  #5 (permalink)  
Per Ardua ad Astraeus
 
Join Date: Mar 2000
Location: UK
Posts: 18,579
Likes: 0
Received 0 Likes on 0 Posts
Not trying to be smart here, but how on earth could that be done in a -300
- as above - very simple - you pull back on the stick.
BOAC is offline  
Old 5th Apr 2011, 15:51
  #6 (permalink)  
 
Join Date: Mar 2001
Location: u.k
Age: 62
Posts: 82
Likes: 0
Received 0 Likes on 0 Posts
Yes i,ve seen a UK registered -300 after a tail strike.
red 5 is offline  
Old 5th Apr 2011, 16:33
  #7 (permalink)  
Per Ardua ad Astraeus
 
Join Date: Mar 2000
Location: UK
Posts: 18,579
Likes: 0
Received 0 Likes on 0 Posts
On a 300, the clue is a very strangely shaped (and short) aft drain pipe
BOAC is offline  
Old 5th Apr 2011, 20:23
  #8 (permalink)  
 
Join Date: Sep 2007
Location: inside of a pretty bustard
Age: 53
Posts: 263
Likes: 0
Received 0 Likes on 0 Posts
the pilots set speeds of zero fuel weight instead of take off weight.as I know it was a 15-20 kts difference which lead to rotate earlier as it could be done.
airman13 is offline  
Old 6th Apr 2011, 00:47
  #9 (permalink)  
Person Of Interest
 
Join Date: Jan 2000
Location: Keystone Heights, Florida
Age: 68
Posts: 842
Likes: 0
Received 0 Likes on 0 Posts
Once again...Basic Airmanship...

Forget the new gen stuff, but the "real" Captain will know when the A/C is ready to fly...or not...

Weight is wrong??? No prob...abort or give it a few more seconds...

Data received from the gate or Ops COULD be wrong...A crew should get their first clue when the breakaway (From the Gate or Ramp) is more or less than normal...Thus the results will follow...
DownIn3Green is offline  
Old 6th Apr 2011, 06:55
  #10 (permalink)  
Thread Starter
 
Join Date: Jul 2005
Location: here and there
Posts: 156
Likes: 0
Received 0 Likes on 0 Posts
I got to know what happened.

ZFW put in the computer instead of TOW.
The result was a Vspeed of 20 nods less than necesasry.
Cabin crew at the back of the plane heard a noise and reported a smokey smell. They called the pilots who didnt really know what happened but decided to go back, as they also felt that somehting was not right during rotation. The initial assumption of the crew was that a tyre burst during take off.
No emergency declared.
capitan very experienced with many many hours under his belt.

Last edited by skytrax; 10th Apr 2011 at 13:14.
skytrax is offline  

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are Off
Pingbacks are Off
Refbacks are Off



Contact Us - Archive - Advertising - Cookie Policy - Privacy Statement - Terms of Service

Copyright © 2024 MH Sub I, LLC dba Internet Brands. All rights reserved. Use of this site indicates your consent to the Terms of Use.