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Old 16th Dec 2011, 00:27
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Gligg
 
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Food for thought

Report: Garuda B733 at Malang on Jul 22nd 2011, hard landing

By Simon Hradecky, created Wednesday, Dec 14th 2011 11:32Z, last updated Wednesday, Dec 14th 2011 11:32Z (The Aviation Herald)

A Garuda Indonesia Boeing 737-300, registration PK-GGO performing flight GA-292 from Jakarta to Malang (Indonesia) with 108 passengers and 8 crew, performed a VOR approach to Malang's runway 35 visually circling to runway 17, however, the aircraft got too high on the approach and turned in too early on base to runway 17 struggeling to acquire the extended runway and glidepath. The aircraft subsequently touched down hard prompting the tower controller to inquire the possbility of a hard landing with the crew. The aircraft was instructed to stop at the end of runway 17 and hold pending a runway inspection, which revealed some metal debris in the touch down zone of runway 17. The aircraft subsequently was cleared to backtrack the runway to taxi to the apron. No injuries occurred, the aircraft received substantial damage including wrinkles of the left wing, a fractured nose wheel hub and damage to the left engine inlet.

Indonesia's National Transportation Safety Committee (NTSC) released their preliminary report reporting, that the training captain (46, ATPL, 14,197 hours total, 5,275 hours on type) was pilot monitoring, trainee first officer #2 (28, CPL, 457 hours total, 457 hours on type) was pilot flying, trainee first officer #1 (33, CPL, 206 hours total, 206 hours on type) was occupying the observer's seat.

Flight GA-292 was number 3 in the arrival sequence to Malang and therefore had been sent into a high level VOR holding for runway 35, active runway was 35.

After the two preceding arrivals had landed, the tower changed the runway to 17 because winds had changed to southerly at 10-15 knots. GA-292 was instructed to leave the VOR holding and commence a VOR let down to runway 35 circling visually to runway 17. After completing the let down the aircraft joined a right downwind for runway 17, turned onto base. When the first officer initiated the turn onto final, the captain assessed that the aircraft was too high for the approach and the turn was too early bringing the aircraft tracking right off the extended center line, and took control of the aircraft. The captain increased rate of descent to acquire the glidepath while at the same time trying to align the aircraft with the extended center line.

The aircraft finally touched down in the touch down zone of runway 17 and rolled down to the runway end to do a 180 degrees turn to backtrack the runway to the apron.

While taxiing down the runway the controller inquired about the possibility of a hard landing, which the captain replied to in the positive. The controller therefore instructed the aircraft to hold before taxiing down runway 35 and had the runway inspected. The runway inspection found metal debris in the touch down zone of runway 17.

After about 10 minutes holding the aircraft was cleared to taxi down runway 35 and to the apron, where passengers disembarked normally.

A post flight inspection found wrinkles to the left hand wing, the nose wheel inner hub was fractured and the left engine inlet cowling was damaged.
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