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Old 24th Feb 2008, 18:44
  #134 (permalink)  
kwachon
 
Join Date: Apr 2006
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Yet again you fail to produce all the information. If you read the official preliminary report you will see important things that were left out in your version and is based on first and second person information not third, in other words ANN's read on the report.

NTSB Preliminary Report.


Accident occurred Friday, February 01, 2008 in West Gardiner, ME
Aircraft: Cessna Citation 525, registration: N102PT
Injuries: 2 Fatal.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

On February 1, 2008, about 1748 eastern standard time, a Cessna Citation 525, N102PT, crashed in a wooded area in West Gardiner, Maine. The private/instrument-rated pilot and one passenger received fatal injuries; the airplane was destroyed. The flight was operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Instrument meteorological conditions prevailed and an instrument flight rules flight plan was filed for a flight from Augusta, Maine to Lincoln, Nebraska. The flight had originated from the Augusta State Airport about 1745.

Representatives of the fixed base operator (FBO) at Augusta State Airport stated that the airplane was fueled and moved from the ramp into the FBO's hangar earlier that morning at the pilot's request. However, the hangar is utilized by a part 121 operator that provides service for that area. The operator canceled its 1630 flight due to the weather conditions and needed the hangar to house its airplane. The Citation was taken out of the hangar and moved back to the ramp area about that time. The pilot was informed of this possibility at time of the request and she stated that she understood that the other customer had priority over the hangar space.

A person identifying herself as the pilot of N102PT called a flight service station at 1701 to file an instrument flight plan from Augusta, Maine to Lincoln, Nebraska, The pilot received a standard weather briefing for the flight at that time. Witnesses stated that the pilot arrived at the airport about 1715, at which time she and the passenger loaded their personnel effects into the airplane, returned a rental car, and paid for the fuel. She and the passenger then boarded the airplane. Shortly after, about 1730, the airplane's engines were started and the airplane was observed taxing. The FBO representative heard the pilot's announcements over the radio in the FBO. He also noticed the airplane was not on the taxiway, but on the grass area on the south side of the asphalt taxiway. At that time the ground was covered with snow and ice.

For the past hour and a half, the weather condition had turned from light snow to freezing rain, and ice was observed covering the cars in the parking lot. The FBO representative noted the pilot did not activate the airport's taxi and runways lights via the common airport frequency radio channel. It was observed that the airplane taxied through a ditch, which was covered with ice and snow. The airplane's engines were heard at a high rate of power about this time. It was later discovered that the airplane's left main tire broke through the ice and became stuck in the ditch. The airplane continued on the grass area after the high engine power was heard. The FBO representative heard the pilot announce the wrong runway (runway 35) that she was planning to depart from. The FBO representative turned on the runway and taxi lights after hearing the incorrect runway announcement. The pilot later announced a change of departure from runway 35 to runway 17, while the airplane was observed back taxing on runway 26 onto taxiway "C" Charlie. About 1745 the announcement for departure from runway 17 was heard; the FBO representative observed the departure at that time.

After takeoff, the pilot contacted the Air Traffic Controller (ATC) and reported that she was at 1,000 feet, climbing to 10,000 feet. ATC requested the pilot to squawk ident on the transponder. Radar contact was made with the airplane when it was about 2 miles southwest of the Augusta State Airport. About one minute later, the pilot declared an emergency and stated, "We've got an attitude indicator failure". About seven seconds later, the pilot announced over the frequency they were not certain which way they were turning. Radar contact was lost shortly after that.

About 1749, local authorities received several 911 calls from residents reporting a possible airplane crash. A short time later, the airplane wreckage was located about 6 miles south-southwest of the Augusta State Airport. One witness stated to local law enforcement authorities that he saw an airplane fly overhead at a low altitude and moments later observed a large explosion off in the distance.

Once again, lets wait and see the official report before making more speculative reasons for this accident. Not once does the word "Confusion" appear in the NTSB version.

(See what I mean sevenstrokeroll, The damage to this thread has mostly been carried out by you. Your credibility regarding your qualifications was lost a long time ago. Not for one minute does anybody believe that you are a "737 Captain for a Major US Airline" so get real and move on).

Last edited by kwachon; 24th Feb 2008 at 18:57.
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