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Old 7th Sep 2004, 02:30
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Milt
 
Join Date: Oct 2003
Location: Canberra Australia
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Canberra Sabotage with a little Preamble
ETPS at Farnborough 1955

Such was the general approach to test flying during those days that it was considered highly desirable that as many pilots as possible, get experience in as many aircraft as possible with a minimum of prior formal conversion. This approach did much to evolve standard requirements for aircraft design and handling in an era when aircraft were developing at a very rapid rate. The constrained restrictions imposed on present generation test pilots arise from a much slower rate of development and an enormous increase in capital costs of aircraft and equipment.

So it was that one day we had a visiting RN Captain fly off in one of our Seahawks. He flew some aerobatics and during the recovery from a loop experienced a terrific bang as a goodly portion of the left side of the cockpit disappeared. He was left with little control over engine power with only a portion of the throttle linkage remaining and was only just able to limp back to Farnborough. He had not seen any other aircraft in the vicinity of the incident but presumed that he had been involved in a mid air collision. The story soon pieced together. A report was made by the pilot of a Hunter who had been flying straight and level at the time that another aircraft had plunged down on his aircraft striking it on the side of the front fuselage and taking out some of his right wing leading edge.

On the side of the Hunter's fuselage was a clear impression of a mirror image of the triangular red sign painted on the sides of aircraft cockpits having ejection seats - "Danger Ejection Seat". This had transfered from the Seahawk to the Hunter during the collision. It became an interesting exercise to subsequently use two models of the aircraft involved to attempt to reproduce the precise sequence of movement of the two aircraft as they became enmeshed for that split second of time. That both aircraft and their pilots survived is indeed remarkable.

At about this time, ETPS took delivery of a B2 Canberra No 867 which had just come through a major overhaul with English Electric at Warton. It was flown into Farnborough by one of the tutors. It was a normal practice then for the TPS engineers to do an acceptance inspection. The senior engineer was meticulous which was as well in that we all placed abnormal reliance on the reliability of the aircraft he and his team maintained and serviced.

Part of his inspection involved climbing through a hatch beneath the rear fuselage to examine the rudder and elevator control push-pull rods which ran along the left side of the fuselage through bearings at about 4 feet intervals. The rods connected directly with the flying controls in the cockpit. They were made from alloy tubing about 1 inch in diameter. The engineer discovered some metal particles scattered down the side of the fuselage in the vicinity of one of the bearings. He initially thought that one of the bearings may have seized and this may have been the source of the metal particles.

On the ground, the mass balance of the Canberra elevator control system caused the elevators to raise to their upper stops so that the control column on the ground was always fully back . The engineer used a piece of cord to tie the control column forward so that he could then inspect the complete run of the control rods. On climbing back into the rear fuselage, he was appalled to find that one of the elevator rods had been cut almost right through. The saw cut had been made so that it would be concealed by a bearing with the controls in their normal ground position.

All hell broke loose. Following an initial ETPS investigation, the police and Scotland Yard commenced a vigorous investigation at the English Electric plant at Wharton.

Some months previously, the wiring looms in the main electronics equipment bay of a Canberra being overhauled at Wharton had been extensively cut by someone using wire cutters. The culprit had not been found. Examination of work records showed that three workmen had worked on both aircraft during the periods in question. Close questioning eventually brought forth a confession by one fitter to both acts of sabotage.

Prior to the sabotage, the culprit had been working on night shifts for which there was an extra pay loading. He was transferred against his wishes to day shifts and decided to take out his resentment by deliberately damaging aircraft on which he was working. He was arrested, charged with sabotage and sentenced to life imprisonment. Hope he served the full term.

I have always taken great care with pre-flight inspections ever since and it was not the last case of aircraft sabotage to cross my path.
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