PPRuNe Forums - View Single Post - The other E.E. classic, the Canberra. (Merged 23rd July '04)
Old 8th Mar 2004, 10:04
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Milt
 
Join Date: Oct 2003
Location: Canberra Australia
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Vertico

Did ETPS at Farnborough 1954 when we had a Canberra join the fleet.

We had no problems with go rounds provided we carefully monitored engine accelerations for compatibility. Ther must have been some close calls after my time.

Was the following Canberra still ther in your time?

At about this time, ETPS took delivery of a B2 Canberra No 867 which had just come through a major overhaul with English Electric at Warton. It was flown into Farnborough by one of the tutors. It was a normal practice then for the TPS engineers to do an acceptance inspection. The senior engineer was meticulous which was as well in that we all placed abnormal reliance on the reliability of the aircraft he and his team maintained and serviced.

Part of his inspection involved climbing through a hatch beneath the rear fuselage to examine the rudder and elevator control push-pull rods which ran along the left side of the fuselage through bearings at about 4 feet intervals. The rods connected directly with the flying controls in the cockpit. They were made from alloy tubing about 1 inch in diameter. The engineer discovered some metal particles scattered down the side of the fuselage in the vicinity of one of the bearings. He initially thought that one of the bearings may have seized and this may have been the source of the metal particles.

On the ground, the mass balances of the Canberra elevator controls caused the elevators to drop to their lower stops so that the control column was always fully forward. The engineer used a piece of cord to tie the control column to the rear so that he could then inspect the complete run of the control rods. On climbing back into the rear fuselage, he was appalled to find that one of the elevator rods had been cut almost right through. The saw cut had been made so that it would be concealed by a bearing with the controls in their normal ground position.

All hell broke loose. Following an initial ETPS investigation, the police and Scotland Yard commenced a vigorous investigation at the English Electric plant at Wharton.

Some months previously, the wiring looms in the main electronics equipment bay of a Canberra being overhauled at Wharton had been extensively cut by someone using wire cutters. The culprit had not been found. Examination of work records showed that three workmen had worked on both aircraft during the periods in question. Close questioning eventually brought forth a confession by one fitter to both acts of sabotage.

Prior to the sabotage, the culprit had been working on night shifts for which there was an extra pay loading. He was transferred against his wishes to day shifts and decided to take out his resentment by deliberately damaging aircraft on which he was working. He was arrested, charged with sabotage and sentenced to life imprisonment.

I have always taken great care with pre-flight inspections ever since and it was not the last case of sabotage to cross my path.
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