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-   -   Icelandair Maxes ferried to Spain with flaps 1? (https://www.pprune.org/rumours-news/626283-icelandair-maxes-ferried-spain-flaps-1-a.html)

golfyankeesierra 14th Oct 2019 14:32


Originally Posted by Mookiesurfs (Post 10594129)
Boeing wanted an all new airplane instead of the Max. Unfortunately, fuel was expensive at the time and airlines insisted on a quicker fuel saving solution. Hence, the Max. Plenty of blame to go around, but airlines drove the decision for the Max instead of an all new aircraft.

Off course Boeing could have started developing a new aircraft a little earlier then 2011. Like 20 years earlier, when the design was already 25 years old😉

infrequentflyer789 14th Oct 2019 15:11


Originally Posted by Mookiesurfs (Post 10594129)
Boeing wanted an all new airplane instead of the Max. Unfortunately, fuel was expensive at the time and airlines insisted on a quicker fuel saving solution. Hence, the Max. Plenty of blame to go around, but airlines drove the decision for the Max instead of an all new aircraft.

More to it than that. Before the MAX announcement, in fact even at the time of it, Boeing was still trying to sort out the 787 development s**tshow. Until it had got the 787 flying and the production problems resolved, done the postmortem and learned the lessons, Boeing was not in the position to develop an all new aircraft, but leaving it that long to announce/start on a program would have lost major 737 customers to Airbus. Also, an all new aircraft would have to compete with the 320neo without any advantage of common type-rating at existing 737 customers.

Boeing found themselves in a corner where the only way out was a re-engined 737, given that they made a hash of doing that it's probably for the best that they didn't try for a complete new aircraft. Boeing weren't put in the corner by anyone else though, it was of their own making with the 787 debacle one of the primary causes.

ph-sbe 14th Oct 2019 16:31


Originally Posted by Gipsy Queen (Post 10592795)
To me, it suggests that there is something fundamentally wrong with the natural balance of the aircraft

Have you noticed any black SUVs parked outside of your home yet? Because I think your are spot on here.

Dan Winterland 14th Oct 2019 16:34

Never trust manufacturer's fuel burn figures for abnormal configurations. I'm sure they make them up using 'best guess' principles and they are always wildly optimistic. I once ferried a VC10 from the West coast of the USA with a main gear leg locked down. We knew from experience the burn figures were a bit on the light side, so we loaded extra fuel as a precaution. Yet, I was still surprised. And we had to endure calls from other aircraft at least every hundred miles of "Hey buddy, do you know you've got a gear leg stuck down".

And once, thanks to a (non flying) misdemeanour, I was first choice for a full flap ferry for a aircraft stuck in Germany. The engineers had been over to fix it, but couldn't find the fault, so it had to be flown back at 120 knots. The type was new in service and we had no experience or figures for this, so we phoned the manufacturers who came up with a fuel burn after an unfeasibly short period of reflection. However, in the cruise, it was soon clear that this figure was plucked out of thin air and was complete bollocks. The result was I had to drop into Coltishall for a hasty refuel. On landing back at base, I absentmindedly went into the after landing sequence and moved the flap lever to up. And the flaps retracted!

However, you can use this to your advantage. A WIWOL colleague was first choice for a gear down ferry in a Lightning from Leuchars to Binbrook - mainly due to being the junior pilot. Thinking out of the box, he worked out that the higher he went, the faster the trip would be. So, skywards he went at just under the gear limiting speed, which was quite high in the Lightning - which I know from experience having refuelled some in flight from a Victor when we had lots of spare gas. To save dumping it, the guys obliged by plugging in with their gear down. Back to the story - what the WIWOL mate failed to appreciate was that after some quite considerable altitude, but still lower than the Lightning's maximum, the gear limiting speed exceeded Mach 1. When English Electric tested the Lightning, no one considered that anyone would ever be daft enough to try to fly it supersonic with the gear down, so WIWOL mate was completely in unknown territory. As it transpired, the aircraft didn't like this very much and demonstrated it's displeasure by departing in a most spectacular fashion. After many tumbles and a dual engine flame out, he finally got it under control with both engines relit at quite a low altitude - too low to climb back up and make it back to Binbrook. So he diverted to Leeming and phoned his boss to tell that the gear down ferry burn figures were too low.

Expatrick 14th Oct 2019 16:38


Originally Posted by Australopithecus (Post 10593851)
Boeing is on the hook for most of it. They have already admitted to an 8 Billion US loss up to the third quarter, so likely this will end up costing them, with the many lawsuits filed, 15 Billion if the Max flies agin in January. At this stage there does not seem to be much chance of that given the world's regulators looking askance at Boeing and the FAA.

15 billion? Is that all? - cheap at twice the price (so VW might say!).

Speed of Sound 14th Oct 2019 17:12


Originally Posted by reverserunlocked (Post 10592739)

The ferry flights are being conducted with Flap 1 to eliminate the possibility of MCAS activating.

Why?

If the AoA vane operation was checked prior to take off and no bird strikes were encountered below the first few thousand feet, the chance of a spontaneous AoA/computer hardware failure occurring in such a small number of flights is virtually nil. On top of that, the first signs of any trim related abnormality would be responded to correctly in seconds by a flight crew who would have a very heightened awareness of the MAX’s problems (the reason for their flight in the first place.) Flying a non-normal configuration could possibly increase the chances of a mishap more than a chance MCAS activation.

MCAS is a real danger to aviation in general, but in a small number of highly monitored flights that danger has got to be minimal.

etudiant 14th Oct 2019 20:02


Originally Posted by Speed of Sound (Post 10594257)


Why?

If the AoA vane operation was checked prior to take off and no bird strikes were encountered below the first few thousand feet, the chance of a spontaneous AoA/computer hardware failure occurring in such a small number of flights is virtually nil. On top of that, the first signs of any trim related abnormality would be responded to correctly in seconds by a flight crew who would have a very heightened awareness of the MAX’s problems (the reason for their flight in the first place.) Flying a non-normal configuration could possibly increase the chances of a mishap more than a chance MCAS activation.

MCAS is a real danger to aviation in general, but in a small number of highly monitored flights that danger has got to be minimal.

Exactly!
Frying pan and fire seems the nearest analogue.

fizz57 14th Oct 2019 21:07


Originally Posted by Speed of Sound (Post 10594257)

MCAS is a real danger to aviation in general, but in a small number of highly monitored flights that danger has got to be minimal.

You're right based on what we know but the JATR report has cast doubt on the unaugmented characteristics of the MAX and I suspect that they know more than they're letting on.

OldnGrounded 14th Oct 2019 21:36


Originally Posted by Speed of Sound (Post 10594257)
Why [fly the ferry flights with flaps 1]?

Probably the regulators aren't taking the chance of letting those flights go without MCAS being inhibited (as far as anyone knows).

Peter H 14th Oct 2019 22:20


Originally Posted by OldnGrounded (Post 10594441)
Probably the regulators aren't taking the chance of letting those flights go without MCAS being inhibited (as far as anyone knows).

If I understand the situation correctly, having flaps out should do two things:
- inhibit the MCAS software
- ensure that the aerodynamic problems which MCAS was designed to mitigate cannot arise (by changing the airflow over the wing). *
So belt and braces [ US suspenders].

Peter

* In https://leehamnews.com/2019/09/27/bj...-wire-part-10/
MCAS is not active on the 737 MAX when flaps are deployed. This is because when flaps are out the slats are out as well and these
diminish the disturbance to the pitch moment curve from the larger and further forward-higher slung engine nacelles.

Big Pistons Forever 15th Oct 2019 00:56

For the last 10 + years Boeing CEO's have made share price and investor short term gains the companies number one priority. In that time they have returned almost 90 billion dollars to investors in dividends and share buybacks. That is money that could have been spent on aircraft development and manufacturing improvements and would have directly improved system safety. This was no accident, it was a choice and is IMO directly responsible for the root cause of the MAX fiasco which is changed a company culture of engineering excellence to a culture of fast and cheap inculcated from the C suite and which has permeated all the way down to the level of aircraft cleaners.

Sadly like example of Exxon Valdez or Deepwater Horizon, Boeing is now another example of what happens when bean counters run a technologically sophisticated and complicated industry sector like it was Walmart.or McDonald's

jack11111 15th Oct 2019 04:21

I believe the Exxon Valdez disaster was not technical failure but total malfeasance by the Master of the ship.

Big Pistons Forever 15th Oct 2019 04:43


Originally Posted by jack11111 (Post 10594567)
I believe the Exxon Valdez disaster was not technical failure but total malfeasance by the Master of the ship.

Actually it has most of the same elements as the MAX catastrophe

When the tanker route was first approved Exxon was required by the US Coast Guard to have many safety measures in place to reduce the chance of an accident.

Exxon immediately worked to water down the requirements to save money. They succeeded in

1) Elimination of the requirement for extra training for the ships officers

2) Elimination of the requirement for an extra officer so that the bridge watch would be well rested for the outbound passage

3) Elimination of the speed limit in the channel. This was the final cheese hole. Under the original requirements the speed was kept low because of floating ice in the channel from the glacier next to the channel. At the low speed the ship could just plow through ice and not be damaged, But to save 3 hrs of voyage time Exxon got permission to go to sea speed in the channel.

At sea speed the ship could not hit ice without sustaining damage and the reason the ship hit Blythe reef which was on the opposite side of the outbound channel, was the tired untrained mate who was maneuvering trying to avoid ice lost situational awareness and by the time he realized he was in trouble the situation was not recoverable

That sound familiar ?

solent 15th Oct 2019 05:46

Perhaps a daft question but for all the 737 MAX aircraft already built, instead of being scrapped could they roll back the aircraft to a 737-800/737-900?

Change engines, remove MCAS etc?

Capt Fathom 15th Oct 2019 06:10


Originally Posted by C172R (Post 10593828)
heard them on the radio couple days ago, flaps1 and FL190 into Alice

From the couple of Silk Air 737s I could find on FlightRadar heading to Alice Springs, normal cruise Flight Levels from Singapore to just before the Australian coast (at Derby), then they descended to FL190 for the remainder of the trip. Looks like CASA put the more limiting restriction in place, but not Indonesia or Singapore.

A and C 15th Oct 2019 06:44

Another option
 
These forums are fed by disaster negative thinking, I offer the following theory as a counter to the usual pessimistic view of those who post on these pages and like some posts above have no hard evidence to base it on.

Boeing must be quite close to a fix for this problem by now and while not wanting to say much until the authorities approve this fix are getting the aircraft gathered together in places that most of the work can be done without using hangar space. After all the weather in Iceland to northern Canada over the winter would considerably slow a work team down without the aircraft being hangared.

gravityf1ghter 15th Oct 2019 06:56

As a side note- Who flew these aircraft? I thought Icelandair laid off all their 73 pilots?

DaveReidUK 15th Oct 2019 07:12


Originally Posted by solent (Post 10594607)
Perhaps a daft question but for all the 737 MAX aircraft already built, instead of being scrapped could they roll back the aircraft to a 737-800/737-900?

Change engines, remove MCAS etc?

No, not a chance.

Australopithecus 15th Oct 2019 07:53


Originally Posted by A and C (Post 10594632)
These forums are fed by disaster negative thinking, I offer the following theory as a counter to the usual pessimistic view of those who post on these pages and like some posts above have no hard evidence to base it on.

Boeing must be quite close to a fix for this problem by now and while not wanting to say much until the authorities approve this fix are getting the aircraft gathered together in places that most of the work can be done without using hangar space. After all the weather in Iceland to northern Canada over the winter would considerably slow a work team down without the aircraft being hangared.

There are zero facilities in the boneyard parking at Alice Springs. BIRK, in the few times I have been in the winter didn’t strike me as that cold...maybe -2°. Air Canada has plenty of hangar space, so what would be the reason to try to avoid using it?

I enjoy a good train wreck story as much as the next disaster maven, but I haven’t yet seen Boeing communicate a cogent plan to address the concerns of regulators and operators. I have my suspicions that Boeing is still trying to address MCAS while leaving the evidently inadequate manual trim system untouched. If a retroactive fix for the trim wheels is mandated, then it follows that Boeing will be exposed to providing 7000+ NG fixes too.

But sure, I fully expect the Max to fly again sometime in my lifetime.

rattman 15th Oct 2019 08:04


Originally Posted by solent (Post 10594607)
Perhaps a daft question but for all the 737 MAX aircraft already built, instead of being scrapped could they roll back the aircraft to a 737-800/737-900?

Change engines, remove MCAS etc?

Zero chance of that happening, only conversion option I could see would be conversion into a freighter, otherwise it would be scrap yard if they cant be made safe



Originally Posted by Capt Fathom (Post 10594614)
From the couple of Silk Air 737s I could find on FlightRadar heading to Alice Springs, normal cruise Flight Levels from Singapore to just before the Australian coast (at Derby), then they descended to FL190 for the remainder of the trip. Looks like CASA put the more limiting restriction in place, but not Indonesia or Singapore.

Seems likely seen a few quotes from CASA and they say it will be a flight profile that prevents MCAS activiating, with flaps out seems to be the only way


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