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-   -   Video Helicopter Crash Rowlett (https://www.pprune.org/rotorheads/645883-video-helicopter-crash-rowlett.html)

SLFMS 26th Mar 2022 06:49

Video Helicopter Crash Rowlett
 
Caution it’s not for the faint hearted.




Agile 26th Mar 2022 08:09

Very dramatic situation on such a beautifull weather day.
I anticipate crash investigators will gather a lot from that tape.

alicopter 26th Mar 2022 08:15


Originally Posted by Agile (Post 11205952)
Very dramatic situation on such a beautifull weather day.
I anticipate crash investigators will gather a lot from that tape.

investigators might use the video ?
So sad. Rest in peace the crew.........

Hot and Hi 26th Mar 2022 08:26

Yes, because it shows they where to look for the (otherwise unscathed) tail plane.

Less Hair 26th Mar 2022 08:39

In the comments here somebody claims to have witnessed the tail rotor coming off.

runway16 26th Mar 2022 09:40

See also Accidents. R22/44 Tail boom events.

R16.

DIBO 26th Mar 2022 09:42


Originally Posted by Less Hair (Post 11205963)
In the comments here somebody claims to have witnessed the tail rotor coming off.

Unless I misunderstood your post, the separated tail can be clearly seen on the video's
https://cimg6.ibsrv.net/gimg/pprune....fb363728d0.jpg


Less Hair 26th Mar 2022 10:21

His statement sounded like it was about a lost tail rotor before the loss of control and the boom being hit.

fdr 26th Mar 2022 11:07


Originally Posted by Less Hair (Post 11205995)
His statement sounded like it was about a lost tail rotor before the loss of control and the boom being hit.

can you point to who/where the comment on the TR comes from please?

One of the eyewitnesses indicates the helicopter was in a hover (OGE...) and then there was a pop....

If the RPM is normal, in the OGE hover the fact that the head is a semi-rigid design, (hybridized from a teetering head to a teetering + coning hinge for root load relief) is basically immaterial. Cyclic inputs on a Robbie like any civil helicopter should be smooth and coordinated, but the hover is not a point that modest cyclic inputs will compromise TPP/tail boom clearance. High speed, very different story. A TR drive failure will get out of sorts in a high hover quite quickly and will result in reduced TPP/tail boom clearance unless the throttle is closed, but there is a few seconds before it gets wild from the inertial moments on the fuselage feeding back into the control system. The video indicates that the NR was likely maintained for the early parts of the event, the blades had not suffered an underspeed event resulting in blade stall (the SN "LOW RPM STALL") the rotors only appear to come out of plane after the pitch over and presumably the engine stoppage from fuel pickup point catching air. This doesn't say one way or the other if the pilot had closed the throttle and entered autorotation, it is probable the event wasn't from an engine failure, however. So, the rotor control head itself is unlikely to have been bad, no pitch link failure, no coning hinge failure, an accidental forward whack on the cyclic is very uncomfortable in the hover but doesn't normally result in a tail strike (there is a neat video somewhere of that being done at a low hover, and stuff happens but the tail didn't get cut off). The same forward whack at 115KIAS is pretty much deadly.

The losses in the RHC are a mixed bag of causes, the fact that it has become the universal training helicopter with the minimal production of any other entry-level chopper other than the Colibri (which has a pretty neat head design) and a smattering of others. The rotor head needs operational care by the pilot, as it did on the B206 and UH1B/H etc... or 2 blade AH1s. They are not forgiving of bad habits, but then, the guys & girls who train the pilots in them take remarkable care to cover those matters, as does the Manufacturer. The RHC Safety Course is a worthwhile course for any person flying them, CoViD notwithstanding.

Sad day for all concerned, fortuitous location of the incident.



Robbiee 26th Mar 2022 17:57

This video mentions that it was a training flight.

SLFMS 27th Mar 2022 00:36

My initial thought was perhaps mast bumping but not severe enough to sever the mast. Before everyone jumps on it it’s just a speculation and I realise that would be unusual.
Another thought I had was if I remember correctly the tail rotor detached at the input in the 44 accident in Broom Western Aus, Perhaps another gearbox failure?

Twist & Shout 27th Mar 2022 03:12


Another thought I had was if I remember correctly the tail rotor detached at the input in the 44 accident in Broom Western Aus, Perhaps another gearbox failure?
Was there a conclusion from the investigation into the Broome crash?
There might be a disturbing pattern occurring.

While not impossible, it would seem extremely unlikely, that pilot error during the reported high (OGE) hover could sever the tail boom.

Catastrophic and unrecoverable mechanical failure is most pilots worst scenario.
When caught on video, the impact is chilling, and can have a deleterious effect on product confidence.
EC225’s are cheap to buy, for EG.
I’m less and less happy to board B737’s (and too scared to watch “Downfall”)

Robbiee 27th Mar 2022 04:44


Originally Posted by Twist & Shout (Post 11206229)

While not impossible, it would seem extremely unlikely, that pilot error during the reported high (OGE) hover could sever the tail boom.

What about Low-RPM Rotor Stall? Perhaps they were doing SWP recovery (the most common reason training flights in Robbys pull into a high HOGE) and something went wrong?

SLFMS 27th Mar 2022 06:12


Originally Posted by Twist & Shout (Post 11206229)
Was there a conclusion from the investigation into the Broome crash?
There might be a disturbing pattern occurring.

While not impossible, it would seem extremely unlikely, that pilot error during the reported high (OGE) hover could sever the tail boom.

Catastrophic and unrecoverable mechanical failure is most pilots worst scenario.
When caught on video, the impact is chilling, and can have a deleterious effect on product confidence.
EC225’s are cheap to buy, for EG.
I’m less and less happy to board B737’s (and too scared to watch “Downfall”)



Yes it was mechanical failure of the gearbox at the input. There had been a vibration reported by the previous pilot with ground trouble shooting not finding any faults. Next flight it failed on vertical departure.
I could be incorrect but if my memory serves me right the tail severed and looked very similar the tail rotor in this video.

Aluminium Mallard 27th Mar 2022 07:45


Originally Posted by Twist & Shout (Post 11206229)
Was there a conclusion from the investigation into the Broome crash?
There might be a disturbing pattern occurring.

While not impossible, it would seem extremely unlikely, that pilot error during the reported high (OGE) hover could sever the tail boom.

Catastrophic and unrecoverable mechanical failure is most pilots worst scenario.
When caught on video, the impact is chilling, and can have a deleterious effect on product confidence.
EC225’s are cheap to buy, for EG.
I’m less and less happy to board B737’s (and too scared to watch “Downfall”)

No report as such, however there was a rumour floating around when Broome R44 happened that it had been towing a water-skier a few days prior to the incident. Broome was different to this one as the blade failed and presumably caused the transmission separation.

For this one supposedly they were training VRS recoveries... perhaps the student staring at the ASI dropped the nose too much with the collective on the floor, the already high RoD leading to freefall, low G then tail off.

I would really like to know what happened but I doubt we will ever find out.

Twist & Shout 27th Mar 2022 07:51


Originally Posted by Robbiee (Post 11206239)
What about Low-RPM Rotor Stall? Perhaps they were doing SWP recovery (the most common reason training flights in Robbys pull into a high HOGE) and something went wrong?

At the beginning of the video the MR RPM appears “normal”. No excessive “coning” or other signs of low RRPM.

Good point though re Vortex Ring. Over controlling in the potential turbulence present during incipient VRS is a possible explanation. EG Nose drops, sudden aft cyclic application.

[email protected] 27th Mar 2022 09:29

Or an over-zealous recovery, lowering the lever and pushing the cyclic forward followed by a check back on the cyclic to control the nose-down.

Simply lowering the lever too quickly will reduce positive g and can even take you to negative - we all know the dangers of that in a Robbie.

SLFMS 27th Mar 2022 10:31


Originally Posted by Twist & Shout (Post 11206229)
Was there a conclusion from the investigation into the Broome crash?
There might be a disturbing pattern occurring.

While not impossible, it would seem extremely unlikely, that pilot error during the reported high (OGE) hover could sever the tail boom.

Catastrophic and unrecoverable mechanical failure is most pilots worst scenario.
When caught on video, the impact is chilling, and can have a deleterious effect on product confidence.
EC225’s are cheap to buy, for EG.
I’m less and less happy to board B737’s (and too scared to watch “Downfall”)


Sorry Twist and Shout the Broome accident hasn’t been finalised, my mistake. It does look like a similar detachment point though.

VRS is interesting possibility especially if it’s known that was the training sortie. A friend of mine ended up on his back in a 500 teaching VRS when it bit back and rolled right over. Luckily it was a 500 as there are not many aircraft you’d get away with that in.

fdr 27th Mar 2022 14:25


Originally Posted by [email protected] (Post 11206316)
Or an over-zealous recovery, lowering the lever and pushing the cyclic forward followed by a check back on the cyclic to control the nose-down.

Simply lowering the lever too quickly will reduce positive g and can even take you to negative - we all know the dangers of that in a Robbie.

On a high inertia rotor you are absolutely correct. On the RHC, in the OGE hover the recovery time is minimal. RHC estimated a tau of around 0.7 seconds for the R-22, which is shorter than the response time required under the FAR for test. It was accepted on the basis that as it is a critical manoeuver the pilot would respond immediately. The R-44 has a better tau but is still not long, the response to an OGE throttle chop is an immediate descent and a rapid loss of Nr. For the R-22, I recorded in an STC series an OGE Nr drop from 104% to 89% in 0.5 seconds, with no perceptible dwell time on the collective. The attitude was recorded for the test helicopter, as well as accelerations, around the CG, blade root loads, both bending and torsion loads, and pitch link loads. Stall Nr was measured for the stable IGE hover at 82%. The mod lowered that to 78% and one configuration got that to 68%. For a Robbie I doubt that anyone teaches or does a delay in lowering the collective in an OGE throttle cut. lowering the collective rapidly itself doesn't give much of a pitch change, the yaw pedal input makes more of a difference to the trim and to the attitude if not corrected quickly. FWIW, my own view is that OGE hover in the RHC is not for the faint-hearted or anyone who is not up to speed. It is required to be trained which apparently this incident was a training flight.


[email protected] 27th Mar 2022 21:20

I'm basing my suggestion on the Gazelle in which I have done OGE hovering and throttle chops but also the Sea King where we trained for forced landing from an OGE hover when we started a lot of FLIR searching.

In both cases, initiating with rapid down collective produced a nose down pitching and a reduction in g.

If this doesn't happen in Robinson aircraft then I'm surprised but happy to have my knowledge improved - not that I'll ever get in one of them again!

Robbiee 27th Mar 2022 22:56


Originally Posted by [email protected] (Post 11206589)
I'm basing my suggestion on the Gazelle in which I have done OGE hovering and throttle chops but also the Sea King where we trained for forced landing from an OGE hover when we started a lot of FLIR searching.

In both cases, initiating with rapid down collective produced a nose down pitching and a reduction in g.

If this doesn't happen in Robinson aircraft then I'm surprised but happy to have my knowledge improved - not that I'll ever get in one of them again!

If you slam the collective down fast in an R22/R44 you will get a brief moment of negative G's,...and I mean brief, its barely one second.

However, I cannot think for the life of me why anyone would chop the throttle in a HOGE in a Robby. In all the years I was subjected to throttle chops never once was it done in a HOGE. Zero airspeed autos like that were always initiated with a smooth lowering of the collective followed by a slow rolling off of the throttle.

tcamiga 28th Mar 2022 07:49

Agree with Robbiee.

First - RIP to the crew, professional investigation in time will tell what actually occurred - but we all wish it had never happened.

To add my bit to the conversation - I have been and still am instructing in the R22 since the early eighties - including original non tip weight blades - and have had no issues with rolling off the throttle for any simulated engine failure to the ground above 100 ft AGL on or outside the HV curve using the following process:

Students have heard all the scary furfies so its about leading them into it slowly following me through bit by bit to keep their confidence.
I do not "chop" the throttle as I do in B47 or other higher energy systems.
Always Student briefed that there will be no surprise throttle chop for their entry - always proceeded with "on the count of three" etc.
Student required to lower the collective at a rate which "splits the needles" - ie- full down - not too fast/not too slow.
Student does not shut the throttle - reasoning is that - in the real thing - there is no need and that a habit learnt at this point against throttle governor and detent spring might slow the lowering of the collective as the wrist action of closing takes nearly a full second of valuable time.
I have the throttle and shut it fully as their collective goes down - always guarding the collective/throttle and pedals.
Hover OGE above 500 ft AGL (HV curve)- nose always pitches down/wait one second for flow to build/ RRPM stabilises around 94% before pointing nose to ground and then building rapidly as airspeed increases. Never an issue.
Student identifies collective full down and calls RRPM at full down no matter entry configuration. Then fly the machine without fixating on RRPM.
Cyclic and pedal input depending on flight condition - through transition/not through transition.(No Low RRPM horn/light system as deactivated at full down collective)

Student to understand from day one that its Main Rotor RPM which holds us up in the air and therefore about learning and implementing the process to initially maintain rotor speed (energy)as much as possible and then complete process to the ground (control inputs) dependant on where positioned in relation to HV curve and environment (wind/landing zone etc)

I always strongly guard the pedals to ensure that if the student inadvertently pushes the left pedal - yes it does happen - it is restricted by right foot on the right pedal.

I guess that the above is what most in this forum do anyway.. but have heard the occasional interesting story such as -

I know of one R22 many moons ago which went inverted and fortunately came back to upright about 100 ft AGL when an instructor was giving a student a hard time and unannounced throttle chops.
At 70 kts and about 900 ft AGL the student caught the instructor by surprise when he put in full left pedal at the same time that the collective went down faster than a speeding bullet.
Nose dropped rapidly/RRPM decay/rolled hard left/went inverted before restored to normal flight / lucky boys.
Engine oil went out the breather and down the tail boom.

Fly safe :)

fdr 28th Mar 2022 11:52


Originally Posted by [email protected] (Post 11206589)
I'm basing my suggestion on the Gazelle in which I have done OGE hovering and throttle chops but also the Sea King where we trained for forced landing from an OGE hover when we started a lot of FLIR searching.

In both cases, initiating with rapid down collective produced a nose down pitching and a reduction in g.

If this doesn't happen in Robinson aircraft then I'm surprised but happy to have my knowledge improved - not that I'll ever get in one of them again!

Crab, not saying that the RHC device doesn't respond to a lowering of collective by starting a descent, if you were powered, but if you had a power loss, then the matter is moot; there is no nicety in lowering the collective at all on the R-22, blade stall occurs by RHC's own analysis in 0.8 seconds, and my own recorded testing is consistent with that, where with an improved blade performance it is still a mind concentrating event. As the Nr collapses (this isn't the nice slow droop of the HH-3, this is more like a descent in a 269, the machine is on its way down, the choice is if you want to have tulip'd blades or want to still have a rotor system, and that requires a prompt lowering of the collective). John Anderson, once he regained his composure suggested that politely lowering the collective was undesirable to his health, that was my intro into whether there was any upper-speed limit in dropping the collective in an OGE hover loss of power.

The R-44 is much nicer to your health than the R-22, but the fundamentals remain the same, the loss of Nr is rapid and has to be responded to by prompt action. I would be more concerned with a case where the machine was not at a heavyweight, and in the power cut the student puts in the wrong pedal, more left instead of pressing right pedal (is USA) that will get a wild ride pretty promptly, and I would think it could compromise the TPP. As long as the rotor is still being driven in autorotation, the control system will function normally. A failure to lower the collective will definitely put the aircraft into zero-g quickly, as the rotor goes into the tulip until impact. As long as the collective is raised, the rotor will decelerate and the rate of deceleration is not trivial. RHC teaches failures every week at their school, and every RHC type trained pilot has experienced the same dynamics. OGE hovering is not for the slow of hand or unprepared driver. Personally, I avoid it whenever I can, happy to do all manner of torque turns, pedal stops etc, IGE failures, but OGE, ill keep the speed up unless there is a compelling reason to go well below ETL, and frankly, speeds above that give a great deal of recovery time as a cyclic loading of the disk trades off speed to Nr. Extremely high speed autorotations are another matter again, there you dont want to "dump a collective" on a robbie, just like you dont on a UH1, that will wind the blades up off the top of the tacho, and gets expensive, that ends up being a gearbox, head and rotor change out. The high speed entry also gives a considerable nose tuck, at the same time as the disk starts to flap back until autorotation is established, (now, that is a bit of maths worth looking at). I tested to 111% VMO at what was supposed to be 90% Nr, but ended up going a little beyond the speed and a little below the Nr. The system once established in autorotation will vibrate considerably in that case, but fly it does. Turning adds vibration depending on the direction of turn. About the only interesting thing in that was while measuring the torsion and bending loads on the rotor blades, and the pitch link strains, found that the entry into autorotation produces momentary loads on the blades and the pitch links that are only matched in the system at one other time, and that is as you touch down. No matter how softly the touchdown is, it is detectable as a load into the disk, which I found interesting. those loads were much more interesting than the steady-state, pitching or rolling loads in the system. That was done on my flight test program, not RHC, but the data says what it says. That was also for clarity, under Part 21 experimental category, with a parachute. Now, the good news is, when you want to work out how to bail out of a RHC, the removal of the blades has an obvious method, doesn't need explosive bolts, just a handful of collective and a twist of the throttle. Do recommend having a parachute on for that though.

Yes, the nose drops, but the TPP follows the control plane, unless there is a big input of cyclic. The thing that concerns me is someone hitting left pedal on entry while in a state of increased anxiety, which may well compromise the TPP/tail boom. A yaw rate from the wrong pedal can lead to the feedback through the control plane and result in an awkward motion of the rotor while the body is rotating underneath the mast, with an offset of the CG to the mast.

All of the above probably goes into the realm of Wayne Johnson to do the maths, or Gordon Leishman, or may be a topic for Shawn Coyle to comment on. Ray Prouty would have given a solution in short order too in small sentences.

Good news though, I'm done with PPrune, you guys fly safely and keep the blue on the top and the needles in the green.

Cheers,






lelebebbel 28th Mar 2022 15:34

fdr, very sad to read that you're done here, your musings were always one of the main reasons i (and probably many others) are reading these forums.

I don't have a lot to contribute other than anecdotes of my experience: an inadvertent left pedal stomp by the student on a simulated power loss in an R44 and R22 does put the machines into an absolutely hair-raising flight state, as you said. It happened to me once in each, during about 10 years of instructing on and off, and in both cases the attitude deviation and rotor RPM loss (mid to low 80s) was what I as a non test pilot would call "extreme". Despite my immediate intervention. I obviously survived both, and there was no damage found, but i can also easily imagine that a slightly different set of entry parameters could have caused structural failures. It would've been interesting to have had a camera in the cockpit, but no such luck.

The instructor in the accident machine has been identified, although i don't know if this information is public yet so i won't go into it. It is a very tragic affair. One thing that is perhaps relevant about the person is that they almost certainly attended the RHC factory safety course somewhat recently.

cavuman1 28th Mar 2022 20:24

fdr, I know many share my sentiments that your contributions here are invaluable. Wisdom, experience, and a sense of humo(u)r are treasured commodities, not just on this website, but in life. You bring all three. We are, after all, pilots and friends who we look forward to meeting one day! I am certain that I speak for the membership when I ask you to reconsider.

- Ed

SLFMS 28th Mar 2022 23:31

I’m wondering if use of the Vuichard recovery technique could have induced a mast bump.
When I used to teach VRS sometimes if you were “lucky” to find it she would sink very quickly, enough to give that sinking feeling in the stomach accompanied with zero or low g. With the power been low there was only a small amount of pedal used to keep the nose straight.
Using full pedal for the side slip on the Vuichard technique and if coupled with low/zero g might be the factor that introduces the roll, especially if the disk is unstable due to VRS.

There is a photo out there where you can clearly see the shear is about where the blade would strike. I assume that would rule out gearbox issue.

Robbiee 29th Mar 2022 15:14


Originally Posted by SLFMS (Post 11207085)
I’m wondering if use of the Vuichard recovery technique could have induced a mast bump.
When I used to teach VRS sometimes if you were “lucky” to find it she would sink very quickly, enough to give that sinking feeling in the stomach accompanied with zero or low g. With the power been low there was only a small amount of pedal used to keep the nose straight.
Using full pedal for the side slip on the Vuichard technique and if coupled with low/zero g might be the factor that introduces the roll, especially if the disk is unstable due to VRS.

There is a photo out there where you can clearly see the shear is about where the blade would strike. I assume that would rule out gearbox issue.

I was thinking along similar lines (only with low-rpm rotor stall). I just did my BFR in a 44 where we went over the dangers of not using enough pedal while doing that new recovery technique.

During one of our practice runs my instructor had me not use enough pedal and we started to spin. I lowered the collective and stopped the spin, but the wind was still making us a bit squirrelly and at one point (before I got everything back under control) the full throttle light came on.

,...and that's not the first time I've skirted with low rpm and the vortex ring state.

Reely340 30th Mar 2022 07:28


Originally Posted by lelebebbel (Post 11206919)
I don't have a lot to contribute other than anecdotes of my experience: an inadvertent left pedal stomp by the student on a simulated power loss in an R44 and R22 does put the machines into an absolutely hair-raising flight state, as you said. It happened to me once in each, during about 10 years of instructing on and off, and in both cases the attitude deviation and rotor RPM loss (mid to low 80s) was what I as a non test pilot would call "extreme". Despite my immediate intervention.

I fly only S300C so pls forgive my lack of Robbie knowledge, but I am curious about that hair-rising flight state mentioned above.
I'd guess : fast yaw to the left due to lack of torque to counter and increased decay of RNR caused by diverting the remaining rotational inertia of the MR to the tail rotor.

Hence: immediate spatial disorientation combined with RNR needle dropping fast, correct?

ShyTorque 30th Mar 2022 08:24

Bearing in mind that the video shows the aircraft travelling from left to right at quite some speed, I’m surprised that there’s so much discussion about VRS.

Or was it was a very badly botched recovery from a vertical descent which resulted in exceeding VNE and subsequent loss of main rotor control?

SLFMS 30th Mar 2022 11:37


Originally Posted by ShyTorque (Post 11207781)
Bearing in mind that the video shows the aircraft travelling from left to right at quite some speed, I’m surprised that there’s so much discussion about VRS.

Or was it was a very badly botched recovery from a vertical descent which resulted in exceeding VNE and subsequent loss of main rotor control?

ShyTorgue are you referring to the video that starts when the aircraft is out of control with the TR severed or is there other footage showing prior to this.
I assume it’s the former in which case there is a lot that could have changed from the initial entry.

I have always been dubious with the Vuichard Technique. Positive forward cyclic to fast accelerating attitude I always found worked best at incipient stages.
Perhaps it’s a technique not suited to teetering hinges.

IFMU 30th Mar 2022 13:20


Originally Posted by ShyTorque (Post 11207781)
Bearing in mind that the video shows the aircraft travelling from left to right at quite some speed, I’m surprised that there’s so much discussion about VRS.

If you turn the video 90 degrees anti-clockwise, the power lines go from vertical to horizontal and the roof will be on the top instead of the right.

wrench1 30th Mar 2022 13:28


Originally Posted by ShyTorque (Post 11207781)
Bearing in mind that the video shows the aircraft travelling from left to right at quite some speed, I’m surprised that there’s so much discussion about VRS. Or was it was a very badly botched recovery from a vertical descent which resulted in exceeding VNE and subsequent loss of main rotor control?

FYI: separate reports state the aircraft was in an OGE hover at the time of the incident. Supposedly the OGE hover was part of the training flight. The CFI was relatively new to the company and the student was an established fixed-wing pilot obtaining his rotor add-on. They've recovered the tail section and the link below shows several shots of it.

ShyTorque 30th Mar 2022 21:09


Originally Posted by wrench1 (Post 11207919)
FYI: separate reports state the aircraft was in an OGE hover at the time of the incident. Supposedly the OGE hover was part of the training flight. The CFI was relatively new to the company and the student was an established fixed-wing pilot obtaining his rotor add-on. They've recovered the tail section and the link below shows several shots of it.
https://www.youtube.com/watch?v=W2HzBCUJvJw

Yes, I've seen the later footage but the video evidence in the first post here shows it travelling at a relatively high speed and in level flight, or possibly even climbing, after the tail assembly had already separated.

AnFI 31st Mar 2022 08:56

Shy that video is deceptive it looks like the helicopter is moving left to right but the frame is 90degrees rotated anti clockwise so the actual path is substantially downwards (not left to right as it appears).

tail does not look chopped to me the break looks too vertical not diagonal slice you never know what happened in the cockpit did the student overpower the instructor? etc etc etc

212man 31st Mar 2022 08:57

Instructor was comms Director with Whirlygirls I see. https://m.facebook.com/whirlygirlsin...al/?__tn__=C-R

wrench1 31st Mar 2022 14:40


Originally Posted by AnFI (Post 11208398)
tail does not look chopped to me the break looks too vertical not diagonal slice

FYI: I believe if you measure distance at the break the M/R blade cut diagonally through only the upper half of the tailboom structure then the lower structure portion failed downward and tore off. And I think you are correct on the OP video that the aircraft motion is vertical due to the camera angle and optical artifacts. There are other reports that support a vertical decent from a hover after the incident.

ShyTorque 31st Mar 2022 14:58


Originally Posted by AnFI (Post 11208398)
Shy that video is deceptive it looks like the helicopter is moving left to right but the frame is 90degrees rotated anti clockwise so the actual path is substantially downwards (not left to right as it appears).

tail does not look chopped to me the break looks too vertical not diagonal slice you never know what happened in the cockpit did the student overpower the instructor? etc etc etc

Thanks, I see it now.

I just looked at an R-44. It appears that the boom separated exactly where an excessively downward flapping blade would contact it. Also, the footage showing the tail assembly being lifted seems to briefly show a sharp edged cut mark near the top of the boom.

Horrible to think about what the occupants must have experienced in those final few seconds.

Robbiee 31st Mar 2022 15:19

Didn't this thread have three pages yesterday? :sad:

RVDT 31st Mar 2022 15:25

Thread creep - mod shifted a bunch of "off topic" to correct topic. You'll work it out.

lelebebbel 31st Mar 2022 15:32


Originally Posted by Reely340 (Post 11207746)
I fly only S300C so pls forgive my lack of Robbie knowledge, but I am curious about that hair-rising flight state mentioned above.
I'd guess : fast yaw to the left due to lack of torque to counter and increased decay of RNR caused by diverting the remaining rotational inertia of the MR to the tail rotor.

Hence: immediate spatial disorientation combined with RNR needle dropping fast, correct?

Hard left yaw, combined with a strong right roll. I'm not going to make an attempt and estimate the roll angle, as i think those estimates are usually far off the mark, and i certainly didn't have time to look at an AI. The rotor decay was instant and likely caused by the disk being tilted forward into the air flow, due to the yaw and roll. I don't have good recollection of the recovery from the first time this happened, but the second time is still in my memory. The correct cyclic and pedal inputs to recover attitude were instinctive, so there was no confusion about the attitude we were in. Basically, full right pedal followed by lots of aft cyclic to recover the revs. Which in itself is not very effective because the extreme yaw really drops air speed, i think i had between 30-40kias left once straightened out. I also still remember the sound of the engine almost choking as i rolled the throttle all the way to the stop, and watched the needles labouring from horizontal back towards their normal position despite the collective being flat on the floor.

​​​​​​If i were to speculate, i think this scenario is one of many possible causes for this accident, but obviously there is no proof one way or the other so far.

Edited to emphasize, one of many possible causes.

For those instructing in these machines currently, you must guard the right pedal to prevent a student from shoving the left one forward. Unfortunately this is difficult to do effectively against a motivated student, especially considering all the other stuff you have to be ready for at the same time. In both cases, the autorotation was not a surprise throttle cut. The students also had done many dozens of autorotations prior, and were preparing for their commercial flight tests. Neither was a fixed wing pilot.


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