Go Back  PPRuNe Forums > Aircrew Forums > Rotorheads
Reload this Page >

30th Nov 2022 crash, Mentone Victoria

Wikiposts
Search
Rotorheads A haven for helicopter professionals to discuss the things that affect them

30th Nov 2022 crash, Mentone Victoria

Thread Tools
 
Search this Thread
 
Old 2nd Dec 2022, 02:27
  #21 (permalink)  
 
Join Date: Feb 2012
Location: All over
Posts: 39
Received 0 Likes on 0 Posts
Originally Posted by SASless
Two hour flight with 25 US Gallons fuel capacity....might be a clue.
Not necessarily SAS. In the photo attached to original post it appears to have 2 tanks which would give it total capacity of 66 gals with an average fuel burn of 12 gph.
donner89 is offline  
Old 31st Mar 2023, 03:48
  #22 (permalink)  
 
Join Date: Mar 2005
Location: N/A
Posts: 5,959
Received 410 Likes on 213 Posts
Final report, still had at least 60 litres of fuel, engine had stopped prior to crash.

Findings
As the helicopter climbed to about 650 ft above ground level, the engine lost power. The reason for the power loss was not determined. A detailed examination of the engine and airframe was not performed, limiting the ability to identify the reason for the power loss

The power loss was not immediately recognised which limited the opportunities for a safe forced landing. During the forced landing, the helicopter did not have sufficient height to reach the selected landing area and collided with rooftops

https://www.atsb.gov.au/sites/defaul...63%20Final.pdf
megan is offline  
Old 31st Mar 2023, 05:52
  #23 (permalink)  
 
Join Date: Nov 2006
Location: After all, what’s more important than proving to someone on the internet that they’re wrong? - Manson
Posts: 1,850
Received 57 Likes on 38 Posts
Hmmmm - another one of life's "little mysteries"?

Can't find a defect report for the failure so .................?

ATSB seem to have taken a hell of a long time and money to basically say - let me see - "nothing".
RVDT is offline  
Old 31st Mar 2023, 07:20
  #24 (permalink)  
 
Join Date: Aug 2000
Posts: 1,949
Likes: 0
Received 44 Likes on 26 Posts
29" on the MP gauge ? The absolute max is 27.2 before you go full throttle. I would suggest if the pilot had got to 29 inches then he would be vastly over pitching and the blades would be coning up at one hell of an angle and the ac would be descending. Had the pilot tried pulling too much power, overpitched and stuffed it in ?( hence a couple of the blades dont seemed to have hit the roof ( as going really slowly ). Would account for not determining power loss !!!
Hughes500 is offline  
Old 31st Mar 2023, 15:38
  #25 (permalink)  
 
Join Date: Jul 2007
Location: USA
Posts: 16
Likes: 0
Received 0 Likes on 0 Posts
Originally Posted by Hughes500
29" on the MP gauge ?
Perhaps this indicates the loss of power. Wouldn't ambient (~29") manifold absolute pressure be consistent with a normally aspirated engine, not running or low rpm per the report, possibly wide open throttle asking for power that's not there?
KMSS is offline  
Old 31st Mar 2023, 16:33
  #26 (permalink)  
 
Join Date: Aug 2000
Posts: 1,949
Likes: 0
Received 44 Likes on 26 Posts
KMSS very possibly ( but the manifold pressure would show that if the engine had stopped) the engine at idle 1600 rpm is around 12 inches of MP but it would appear that from the investigation there was not a problem with the engine ????
Hughes500 is offline  
Old 31st Mar 2023, 16:50
  #27 (permalink)  
 
Join Date: Jul 2007
Location: USA
Posts: 16
Likes: 0
Received 0 Likes on 0 Posts
H500 - Yes, not much to go on.

I noticed this in the report: "...a visual inspection of the engine cooling fan and fan shroud indicated that the engine was not running at the time of the accident. The degree of damage to the rotor blades also indicated that the engine was providing little or no power."

I'm not a helicopter pilot but I wondered if the 269C has a governor which would have been opening the throttle as power output and engine RPM decayed for unknown reasons, leading to the increasing MAP...
KMSS is offline  
Old 31st Mar 2023, 21:59
  #28 (permalink)  
 
Join Date: Aug 2000
Posts: 1,949
Likes: 0
Received 44 Likes on 26 Posts
I find it difficult to believe that a more serious investigation of the engine lack of power wasnt performed.Is there a root cause of engine problems with HIO 360D1A's ( i would like to know my school uses 3 of them ). The engine must have been providing some power otherwise the student would have to have been in immediate autorotation which doesnt seem to be the case. Looking at the pictures the engine area and scroll look pretty intact
Hughes500 is offline  

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are Off
Pingbacks are Off
Refbacks are Off



Contact Us - Archive - Advertising - Cookie Policy - Privacy Statement - Terms of Service

Copyright © 2024 MH Sub I, LLC dba Internet Brands. All rights reserved. Use of this site indicates your consent to the Terms of Use.