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We should not point fingers

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Old 3rd Mar 2009, 18:23
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We should not point fingers

but has this gone to far?

Ore. firefighter's mother sues helicopter company - NewsFlash - OregonLive.com

Just read in the Oregonian that the mother of one killed in California helicopter crash has sued several helicopter companies for neglect.

Why?

Am I out of line to post this?
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Old 3rd Mar 2009, 18:43
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Let's put a face to a bit of text.....we are talking about real people when we do the accounting.



Family of dead firefighter sues helicopter maker, others - OregonLive.com

The Iron 44 Incident - The Oregonian Extra - OregonLive.com

Last edited by SASless; 3rd Mar 2009 at 19:05.
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Old 3rd Mar 2009, 20:22
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To add to SASless, lets put the rest of the names here too:

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Old 3rd Mar 2009, 21:07
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Gordy,

I knew Roark from days past.....another Good Guy gone!

Knowing him like I do....he is probably ragging on Elvis and keeping folks laughing!

Meeting him was one of the bright spots of my flying career.
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Old 3rd Mar 2009, 21:29
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Too soon?

It's undeniably sad. Always is.
If the cause were linked to an avoidable design flaw in the helo, then yes, of course Sikorsky would be at fault.

BUUUUT....

LAX08PA259

NTSB's report is still only a Prelim. So while the cause of the crash may be blindingly obvious (which it doesn't even seem to be that in this case), its not really official until NTSB sez so.

So no, I have a hard time with this kind of lawsuit. It just seems like a no-good shotgun lawsuit. Whether originated by the grieving mother or a money-hungry lawyer telling her "you could make a big buck off this!" What if it were to come out later that the accident was pilot error? then who does she sue?

Too many what-ifs and don't really want to speculate. It's sad, I feel bad for the family, and yes, there were similar accidents in appearance, but we just don't know the actual cause yet.

Blah.
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Old 3rd Mar 2009, 21:40
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SAS---Never met Roark, although one of the ladies in our office worked with him at Columbia. I did know Jim--he carded me last year and also worked for many years where I now work .

I hauled all the "contaminants", (jet fuel soaked dirt), from the site last October...Because the site is in a designated "wilderness area" the task had to be completed with minimum impact. We flew in a Hazmat team who worked with hand tools for a week filling 1,000 lb bags with "contaminated dirt" which we slung off. We had a 36nm round trip each flight, (could not land in the "wilderness" area), for a total of 90 seperate flights and over 50,000 lbs of dirt. The site is now "re-habbed" back to its natural state.

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Old 5th Feb 2013, 02:13
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Former employees of carson helicopters indicted over fatal iron 44 fire crash/

More Here

Two former employees of Carson Helicopters are facing 20 years or more in prison for charges related to the crash of a helicopter in 2008 that killed nine people (seven firefighters and two crew members) as it attempted to take off from a remote helispot on the Iron Complex or Iron 44 Fire in northern California.

Last week a federal grand jury in Medford, Oregon indicted Steven Metheny, 42, former Vice President of Carson, and Levi Phillips, 45, the former maintenance chief of the company, for charges of conspiracy to defraud the United States which could earn them up to 20 years in prison if convicted.

Metheny was also indicted in 22 other counts of mail fraud, wire fraud, making false statements to the Forest Service, endangering the safety of aircraft in flight, and theft from an interstate shipment. In addition to the 20 years for conspiracy to defraud charges, he could also get a maximum sentence of 20 years for every mail and wire fraud count, 20 years for each endangering the safety of aircraft in flight count, 10 years for the interstate theft count, and up to five years for each false statement count.

According to the findings of the National Transportation Safety Board in 2010, there was “intentional wrong-doing” by Carson Helicopters that under-stated the weight of the Sikorsky S-61N helicopter and over-stated its performance in the documents they provided to the USFS when bidding on $20 million in firefighting contracts for seven helicopters. As a result, when the helicopter attempted to take off from the helispot on the Iron 44 Fire with firefighters and a flight crew of three, it was over the allowable weight even before the firefighters boarded the ship. The helicopter crashed into some trees and caught fire, just after lifting off.

Killed in the crash were pilot Roark Schwanenberg, 54; USFS check pilot Jim Ramage, 63; and firefighters Shawn Blazer, 30; Scott Charlson, 25; Matthew Hammer, 23; Edrik Gomez, 19; Bryan Rich, 29; David Steele, 19; and Steven “Caleb” Renno, 21. The copilot and three other firefighters were seriously injured.

In March of 2012, a jury ordered the manufacturer of the helicopter’s engines, General Electric, to pay $69.7 million to William Coultas (the surviving pilot), his wife, and the estate of Roark Schwanenberg (the pilot who was killed).

After the crash the U.S. Forest Service canceled their contract with Carson Helicopters. The company then surrendered their FAA Certificate which is equivalent to an operating license. After that they received a contract for seven S-61s to fly for the military in Afghanistan as a subcontractor for the company formerly known as Blackwater Worldwide, which was renamed “Xe”. In February 2010, Sikorsky announced a joint venture with Carson to supply up to 110 modernized S-61T helicopters to the U.S. government, primarily for the State Department.

The U.S. Attorney’s office in Oregon is working with the Offices of Inspector General for both the Department of Agriculture and the Department of Transportation in Portland, Oregon and Seattle, Washington, and the FBI and the IRS in Medford, Oregon in the investigation and prosecution of this case.
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Old 5th Feb 2013, 09:59
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This is very good news.

I shall hope the prosecution is successful and the those two spend the rest of their lives in Prison.

Some very good Men died as a result of their actions.

I refused to dummy up some paperwork on an aircraft one time....and some folks wondered why I refused. Hope they understand now.

Last edited by SASless; 5th Feb 2013 at 10:02.
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Old 5th Feb 2013, 15:59
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In all four cases, the helicopters crashed as they were lifting off, caused by a failure of a clutch mechanism that connects engines to the helicopter's five main rotors, attorneys for the pilots and their families argued in courts in Oregon, Tennessee and British Columbia.
*Sigh.*
Can't journos fact check and get their terms straight?
Rotor blades, of which an S-61 has five, are part of the main rotor(or main rotor assembly) of which the S-61 has one.
Their profession is words, and they can't get the words right.

Aside: sprag clutch failure?
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Old 5th Feb 2013, 17:15
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In March of 2012, a jury ordered the manufacturer of the helicopter’s engines, General Electric, to pay $69.7 million to William Coultas (the surviving pilot), his wife, and the estate of Roark Schwanenberg (the pilot who was killed).
Several times the NSTB report states the engines were performing normally and did not contribute to the accident ..... so why would General Electric have to pay the $69.7 million ?? Strange !!
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Old 5th Feb 2013, 17:33
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Aside: sprag clutch failure?
Read the report. Both engines were at max Ng all the way to impact.

Last edited by 212man; 5th Feb 2013 at 17:34.
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Old 5th Feb 2013, 19:20
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With you there Arnie, if both engines worked as advertised why did GE get stitched for millions?
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Old 5th Feb 2013, 19:40
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Probably because of this:

Jury awards $70 million for helicopter crash on Iron Complex fireWildfire Today

The whole fiasco stinks. Not only did the engine saga stink, but the Carson inditement did too. Apparently here we had an operator flying duff engines on duff airframes. WTF

And there's me thinking Carson were a reputable company. The Carson blade kit has transformed S61 and SeaKing flight characterisitics.

Please, someone, tell me there is no connection between the Carson inditement and the 'other' Carson phenomena???
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Old 5th Feb 2013, 19:59
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Found this on Carson's facebook page

"On 5 August 2008 a Carson Helicopters Sikorsky S-61N crashed on take off. According to the NTSB, nine people were killed. These were the pilot-in-command, Roark Schwanenberg, 54, of Lostine, Forest Service safety official Jim Ramage, 63, and seven firefighters: Shawn Blazer, 30, of Medford; Scott Charlson, 25, of Phoenix, Ore.; Matthew Hammer, 23, of Grants Pass; Edrik Gomez, 19, of Ashland; Bryan Rich, 29, of Medford; David Steele, 19, of Ashland; and Steven "Caleb" Renno, 21, of Cave Junction. The copilot and three firefighters escaped the burning wreckage and survived with serious injuries. The NTSB's preliminary report determined that the cause was a loss of power on take off probably caused by an engine failure. In January 2010 the NTSB issued its final report finding that the probable causes of this accident were several actions by Carson Helicopters: intentional understatement of the helicopter’s empty weight; alteration of the power available chart to exaggerate the helicopter’s lift capability; using unapproved torque in performance calculations; and that additional causes were insufficient oversight by the U.S. Forest Service and the Federal Aviation Administration. Relatives of the victims concerned by the change in the NTSB report filed a lawsuit against General Electric and on March 27, 2012 a jury unanimously ruled that the primary cause of the accident was the failure of the GE CT-58 engines."
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Old 5th Feb 2013, 20:15
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OH Hell Yes.....By all means let's point fingers!

When a couple of guys falsify documentation to obtain contracts and later those material falsifications lead to fatal accidents...then by all means lets point our fingers at them. What's more, even if they do not wind up in Federal Prison for their felonious conduct....let's run them out the industry for good.

Here is the NTSB Accident Report.


http://www.ntsb.gov/doclib/reports/2010/AAR1006.pdf


Note the explanation about how the empty weights were falsified and also how the bogus performance charts were created. The fact the USFS failed to catch the understatement until the NTSB pointed it out to them is also indicative of how they do their business in the contracting office. There are some bureaucrats in the office that need removing but then they are all good civil servants.

The USFS Check Pilots I have dealt with have all been professional and knowledgeable in their work and to the Man were very pleasant to deal with.

The lying scoundrels not only lied to the Forest Service but worse they lied to their own Pilots and the passengers they carried.

When people burn to death as a result of your actions....you deserve no mercy.
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Old 6th Feb 2013, 01:11
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SAS, you really like to use absolutes. There are a lot of fingers to be pointed.

There is a lot of data in that report, takes a while to get through it.

Thomas:
The whole fiasco stinks. Not only did the engine saga stink, but the Carson inditement did too. Apparently here we had an operator flying duff engines on duff airframes. WTF
The engines were good, but asked to do more than they were capable of. Topping is topping, that's all you get.

1.18.2 Pilot Interviews
NTSB investigators interviewed five former CHSI pilots following the accident. Four of the pilots reported that, while it was not normal to reach engine topping during passenger-carrying operations, it was a more common occurrence during water-hauling or logging operations. One pilot stated that, “when you reach topping, you jettison. This is a daily experience that pilots deal with when carrying water rather than passengers.” Another pilot stated the following:
Logging and passenger operations provide an entirely different environment. In logging, the aircraft has no interior or seats, bare metal and wiring, and carries only what is necessary for the operation. Time is money, and logging is a timed event paid by board foot. By contrast, passenger operations are [paid] by the hour. You cannot jettison loads. Topping is normal in logging, but only as an emergency measure. It is not normal with passengers, where calculations are based on takeoff power rather than topping.
In earlier times, pilots would try to carry more than the helicopter was capable of carrying. Therefore, load calculations are now made as a guide and are rigorously held to in Part 135 operations. With firefighting operations, when carrying water, these calculations are not etched in stone. You trim for comfort, check power
74
NTSB Aircraft Accident Report
75
available before loading water, then take on water. For example, you pull in 81% torque as the best power before drooping, therefore at 71% torque you stop loading water.
The pilots reported that, typically, on water-dropping missions, an in-flight power check
I agree that the Carson execs acted criminally and should be punished as such. Their acts were designed to deceive. Again, not the only operator out there that does this, by far.

I've had another operator try the same things on the same airframe.

The problem is, to quote you from another thread:

ass, tin, ticket
What were the guys thinking using topping on one take-off after another to struggle over the trees and saying the power is "good"? Clearly there was culture of exceeding limitations that they either agreed with or had aquiesced to.

I agree that the falsified charts would lead them into the problem, but they have access to an unaltered RFM. That was a huge first hole in the cheese (criminally so)and if they had restricted themselves to RFM t/o limits, they would have landed back and kicked some guys out.

NTSB:
During the two previous departures on the day of the accident, the pilots had the opportunity to realize that the helicopter was overweight or at least that it was not performing in a manner consistent with the load calculations. The NG gauges would have shown that the engines were being operated in excess of the flight manual takeoff NG limit of 100 percent (shown on the NG gauges as a red line) and were at topping power. Additionally, the droop in NR would have been audible to the pilots and visible on the triple tachometer. Nonetheless, neither
...
pilot mentioned that the engines were at topping, even though the load calculations showed that they should have been well below the helicopter’s maximum performance capabilities. Further, neither pilot called attention to the discrepancy between the predicted and actual performance of the helicopter or suggested postponing further flight until the discrepancy could be resolved.

The PIC had accumulated the majority of his experience flying helicopters in the logging and firefighting industries. As revealed by the comments of other S-61 pilots, the operating procedures are significantly different when carrying logs or water than when carrying passengers. In both logging and water-dropping missions, the pilots do not routinely rely on load calculations. In logging, the operation of flights is driven by the maximum power capabilities of the helicopter as indicated by the torque gauges, and pilots consistently load the helicopter until it reaches its maximum performance capability, knowing that they can jettison the load and instantaneously decrease the power required to hover or climb.
I can't believe that the engine manufacturer is being tagged to pay out on this. Insane.
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Old 6th Feb 2013, 04:02
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I agree about the Jury finding....the NTSB clearly stated the Engines were not the cause and were operating correctly. I am sure upon Appeal the Jury Verdict shall fail.

Now that Federal Indictments are done....the two guys on the hook will have to make some decisions about how to respond to those charges. I am sure they are lawyered up and will be receiving some very expensive Legal Advice.

They are going to have consider some sort of Plea Bargain as I can bet the US Attorney would prefer to settle this out of court as the FAA and USFS are going to be wearing a lot of Egg on their face should it go to Trial. Likewise, when the civil proceeding starts....as you know the Families are going to go after these two and Carson now that the two executives are under indictment.

The major cause of the accident is the false performance data and the false Weight and Balance information.
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Old 6th Feb 2013, 04:36
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SASless wrote,

"The major cause of the accident is the false performance data and the false Weight and Balance information."

Nonsense.

One of two things happened here:

(1) Whether flying a 61 or any other helicopter one must first determine whether or not one has enough power to get out of the confined area. I have flown 61's many hours at high DA's and Ng topping is always an issue. A number on a piece of paper did not cause this accident - but lousy judgement may have.

(2) The co-pilot insists he saw a torque split as they were coming out of the hole. If this was the case, it is a straightforward power loss on takeoff. There is also the issue of a (perhaps) incorrect fuel control overhaul at Columbia. This story ain't over yet.

Finally, this aircraft was purchased by Okanagan Helicopters in 1966 and we put over 40,000 hours on her. I personally flew her more than 3,000 hours. Sad end to a grand old Lady.

Last edited by oleary; 6th Feb 2013 at 04:47.
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Old 6th Feb 2013, 04:53
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Oleary,

If the Co-Pilot saw a torque split....why does the NTSB Report state both engines were functioning normally and bases that statement upon the CVR data and the engine examination after the crash and makes no mention of that statement by the Co-pilot?

Where are you getting your information about the improper overhaul at Columbia?

While you at CHC were flying that bird at "Topping" all those forty thousand hours....were you still using standard Sikorsky TBO data based upon their initial flight testing for certification or did CHC modify that data to reflect all those hi-power settings and cycles and wear and tear from unusual forces caused by Logging and Water hauling? The aircraft TBO's on drivetrain and dynamic fatigue loaded parts are impacted by the power vs time at power spectrum as I am sure you are aware.

Carson by the use of Plus Spec Power settings and higher weights and the use of 2.5 minute OEI power for takeoffs really loaded up the aircraft in that regard and some thought might be given to what effect that has on TBO's.

As you seem to say you at CHC operated the aircraft and had Topping issues....what techniques did you use to avoid "Topping Out"? Did you limit weights, abort takeoffs that caused you to go beyond the limits for Ng...or did you do as most Loggers do....carry all the weight you could even if it meant drooping some Nr so long as you could clear the barriers?


I posted the NTSB Report earlier if you want to review that and point out any errors you may think they made for us.

Last edited by SASless; 6th Feb 2013 at 05:11.
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Old 6th Feb 2013, 05:43
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Caveat: I knew Jim Ramage the inspector pilot on board, he used to work where I now work, I know his widow. I did not know Roarke or Bill, but I know lots of people who do, and all speak highly of them. As shown above, I flew most of the clean-up operation.

I am not a party to any other part of the investigation or aftermath, so, let me point you towards some clues as to what is being discussed, the 15 points raise serious questions:

A helicopter crash that killed nine continues to raise questions more than two years after the accident. The accident occurred on August 5, 2008 near Weaverville, California as a Sikorsky S-61N helicopter took off from a rugged mountaintop clearing ferrying firefighters to a wildfire in the Trinity Alps Wilderness. Seven contract firefighters, a U.S. Forest Service safety inspector and the pilot were killed.

On Dec 7, 2010 the NTSB met to determine the cause of the crash and make safety recommendations. Their recommendations raised questions about the safety of government aircraft and documents indicated the chopper was overweight.

Two victims' families are speaking out through an attorney against those findings by the NTSB. The Coultas and Schwanenberg families charge the NTSB changed its initial conclusion from an engine failure to a weight issue because the report was written by the wife of the NTSB investigator that was responsible for the security of the parts, according to Gregory Anderson of AndersonGlenn, LLC.

Bill Coultas, who was severely injured in the accident and Christine Schwanenberg, wife of Roark Schwanenberg, who was killed in the crash believe there should be an impartial and unbiased investigation and that there is a conflict of interest with this report.

Both men were pilots of the helicopter, employed by Carson Helicopters. The families, through Anderson, would like to make the following facts public:

1) The original cause of the accident found by NTSB investigators was the loss of power from the No. 2 engine due to a well known issue over fuel filtration. The NTSB reached this conclusion following the inspection of the engines at a Columbia Helicopters repair facility in Aurora, Oregon on August 14th, 15th and 16th, 2008, just nine days following the August 5th accident. Columbia, an approved fuel system contractor for repair of the GE CT-58 engines involved in the accident, was the last party to have physical control of the parts. NTSB investigator Jim Struhsaker turned over control of the Fuel Control Units to Columbia on August 16th, 2008 for shipment back to the NTSB. Carson was not present, having left the inspection on the 15th to attend memorial services of the victims.

2) Columbia, GE and Sikorsky are all financially interested parties as defendants in multi-million dollar lawsuits brought by the victims and their families.

3) The Flight Data Recorder (FDR) was functioning and had 77 hours of data recorded. The NTSB investigators could not coordinate the timeline of the cockpit voice recorder with the FDR data so they labeled it "invalid" or "irrelevant". In fact, it contains information of heading, altitude and engine performance. No attempt was made to integrate this data after August 16th 2008, when the fuel system components were lost.

4) GE, Sikorsky and Columbia had been facing allegations of a dangerous defect regarding the fuel control units, specifically, stuck stator vanes due to a contamination of Pressure Regulating Valves (PRV) and clogged filters, which when clogged to a certain degree, allow the CT58 to continue to operate through the use of an emergency by-pass valve. When this occurs, unfiltered fuel is allowed into the Fuel Control Unit, and results in contamination of the system. The diameter or "clearance" of the diaphragm of the PRV is only six (6) microns in thickness. The filters in use in N612AZ, the S-61 involved in the Trinity crash, as well as the four preceding crashes from this issue, were for forty (40) micron contaminants. The US military identified the filtration issue in its S-61s in the 1990s and switched to the finer, 10 micron filter. Following the upgrade, military S-61s no longer had fuel filter issues.

5) The day following the accident, email exchanges between GE and Sikorsky engineering departments raise filtration immediately after being notified about the accident.

6) The S-61N involved, had a maintenance history that included concerns over stuck fuel system components due to fuel contamination. The maintenance history of the S61N was not considered in the Board's findings.

7) There have been four prior accidents involving the CT58 fuel system in the S-61 where fuel contamination was cited as the cause, including a 2004 detailed investigation by the Canadian Transportation Board into an S-61N firefighter crash where it determined the GE CT58 fuel filter issue was the probable cause. The prior accidents were not considered by the Board.

. 8) The sole evidence that the No. 2 GE CT58 engine in N612AZ was functioning nominally was a sound spectrum analysis prepared by GE using Sikorsky charts of the sound signature of the planetary gears in the S-61 transmission and the sound signature of the gas generator blade rpm. In order to determine whether the No. 2 engine was developing its full power, the NTSB would need four facts: first, "Nr" or rotor blade rpm; second, "Ng", or gas generator (compressor) speed; "Nf" or power turbine speed; and finally, "T5" or turbine inlet temperature, which shows the amount of heat developed in the CT58 combustion chamber (for the CT58-140 installed in this S-61N configuration, that should have been 721 degrees). The NTSB did not determine the second and third required parameters and so could not have determined whether the No. 2 engine had achieved "topping" or top rated horsepower.

9) The sound spectrum analysis is the only "quantitative" data for the conclusion that the No. 2 engine had not failed. Absent this GE/Sikorsky analysis, all of the NTSB conclusions are speculation. Objective facts supporting an engine issue include the No. 2 torque gauge found post accident with a "split" of 30% from No. 1. The NTSB theorized this could be from a power loss but wiring schematics show this to be an A/C powered gauge that would have frozen with a sudden loss of power, not wound down. Even if it had been a DC powered gauge, there would not have been a split: both gauges would have wound down to zero torque. The Emergency Throttle for No. 2 was found in the partially opened position. Bill Coultas and a second eyewitness confirm that he was attempting to open the No. 2 Emergency Throttle after he saw the torque split on the gauges. The only reason to do so was a concern by the flight crew with fuel. The Emergency Throttles are gated and require significant force to move to an open position. Bill Coultas testified they lost power and noted the loss of rotor speed before they hit any trees.

10) Comparison of the markings on the stator vanes are significant.

11) The NTSB ignored Bill Coultas' testimony that they had cleared a 50' (AGL) tree before losing power and descending into the #1, #2 and #3 trees documented to have been hit by the rotor blades in the report. The GPS plot of N612AZ's course, combined with the (NTSB commissioned) survey of the area, prove unequivocally that N612AZ climbed to 60' or more before losing power. The significance is that in sloping terrain (the NTSB survey shows between 8 and 20 degrees of ground slope once the helicopter left the immediate landing area of H-44), the "Hover Out of Ground Effect" ("HOGE") altitude could not have been more than 30' (AGL). To get to an altitude of 60-70' AGL, the helicopter had to climb out of ground effect, which renders the theory of an overweight issue as a cause, speculative. Succinctly, if the helicopter was grossly overweight, it would have never been able to climb out of ground effect (the cushion of air between the ground and the whirling disk of the rotor blades), but would have "settled" back down. This effect would have been immediately noticed by the flight crew. It is a matter of mathematical certainty that an S61N at this density altitude could not have climbed out of ground effect and over a 50' obstacle if it were in a gross overload situation. As a matter of record, N612AZ did climb out of ground effect and transition into forward flight, and climbed over a 50' obstacle. Weight was not the issue.

12) The NTSB asks the public and the aviation community in particular, to believe that a Pilot-in-Command (Roark Schwanenberg), a Second-in -Command (Bill Coultas) and a Forest Service Check Pilot (Jim Ramage), with a combined total of 29,000 hours of helicopter time: lifted off from H-44; never noticed any weight problem; never noticed the helicopter settling; never felt it reacting sluggishly; never considered putting her back down; never thought of their own safety (all three had families –Schwanenberg and Coultas with minor children); ignored the lives of the nine firefighters in the back, and essentially flew directly into the trees.

13) The NTSB took Bill Coultas' statement that "we had plenty of power" and presented it as though he was stating the condition of the helicopter as it was crashing. The transcript of his post-accident interview makes clear he was stating that he and PIC Schwanenberg had determined that they would have plenty of power for the last (crash) flight as they performed the preflight calculations, based on the observed temperature and winds. By taking the SIC's statement out of context, the NTSB presented it as conformation that the engines were producing full power. This is contrary to sound investigation techniques requiring an unbiased and impartial evaluation of the testimony.

14) The NTSB Materials Report (taken off the public docket in violation of the NTSB's "transparency" policy issued in June of 2009), was the result of complaints by the victims and the aircraft's owner/operator, Carson Helicopters to the NTSB and to members of Congress, including Oregon Representative Pete DeFazio. After Carson's request for a congressional investigation into the loss of the parts, the NTSB investigation shifted to an investigation of Carson and the weight issue. Prior to Carson expressing concerns to Congress over the parts, the focus was on the engine filtration issue.

15) In the GE/Sikorsky prepared "worst case" simulation, the helicopter was alleged to have weighed 19,008 lbs. The Sikorsky performance charts, even using the "stock" rotor blades instead of the composite, high performance blades on N612AZ, show that at this altitude, temperature and wind, the helicopter could lift over 19,100 lbs. Assuming every fact in favor of the NTSB/GE/Sikorsky simulations, N612AZ could have and did fly from H-44 until the No. 2 engine failed.
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