Originally Posted by Lead Balloon
(Post 11142278)
In fairness, the witness is quoted as saying what the pilot said. Either the witness misheard the pilot stating that he tried switching fuel tanks, or the pilot was a bit confused...
Or maybe the reporter misheard or misquoted the witness... Happily we should hear first hand soon . . |
Just reported-engine had flooded carby...
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Originally Posted by chimbu warrior
(Post 11142441)
https://edition.cnn.com/2021/11/14/u...cue/index.html
I think this one qualifies as the ditching of the day; didn't even appear to get his feet wet. The reason the pilot isn't wet and doesn't have a life jacket on is that the aircraft is sitting on the bottom. The waters off Cedar Keys Florida are very shallow. |
Originally Posted by The Banjo
(Post 11143157)
Just reported-engine had flooded carby...
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Spin
The situational awareness and quick actions of the Marine Interdiction Agents and Sheriff's Deputies prevented a possible human tragedy," said Michael Matthies, Deputy Director of Marine Operations. "We are thankful we have the proper resources and trained personnel to perform when incidents like this present themselves. We completely missed seeing an aircraft crash nearby on a perfectly clear and calm day, then happened to accidently come across it, and were able to get close enough to pull the pilot who had rescued himself on to our boat. |
The reason the pilot isn't wet |
Oi rekkon OI'd be a fair bit 'soaked' in the next hour or so tooo.....
Cheeerrrsss...... (Hic) |
Originally Posted by Progressive
(Post 11143313)
On an Injected 540?
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Originally Posted by Oodnadatta
(Post 11142301)
He may have been trying to switch to the Backup Thronomister Motor but unless there was sufficient Chemtrail he would not have been able to maintain height.
It's just a theory but others have been caught out before. |
Now that the finest “Aviation Experts” in Australia (Except GT) have suggested the most likely cause of this event I was wondering if those in charge have been able to download the contents of the “Black Boxes” from the aircraft. This would help stop the speculation and the media could report the actual cause.
Cheers, Oods. |
‘Oodna’, I’m surprised that your unaware that the black box has in fact been analysed at the ATSB’s Oodnadatta depot. It’s probably sitting on a bench just round the corner from your place.
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This was a turboencabulator failure, without doubt. Usually it's fretting on the prefabulated amulite base.
Classical symptoms. |
Geez Megle2, I dropped the ball on that one. Not many corners around here but I know where you mean.
I was distracted trying to figure out why a WA couple got bogged in the Simpson Desert. The Oodnadatta refueller can give you the full story. Cheers, Oods. |
This was a turboencabulator failure, without doubt. Usually it's fretting on the prefabulated amulite base. |
Unlike the pilot who probably did a weather check before flight, the Simpson campervanner obviously did not.
Bit of a transcontinental shift in thread … from surf to sand. Van recoverable, Tobago beyond it. |
Originally Posted by aroa
(Post 11143967)
Unlike the pilot who probably did a weather check before flight, the Simpson campervanner obviously did not.
Bit of a transcontinental shift in thread … from surf to sand. Van recoverable, Tobago beyond it. |
GeeeeSus Gerry , I think you've GOT-IT.
"That would NEVER 'appen in GA" ......Well.....Hardly ever...???? Cheeerrrssss |
Originally Posted by aroa
(Post 11143967)
Unlike the pilot who probably did a weather check before flight, the Simpson campervanner obviously did not.
Bit of a transcontinental shift in thread … from surf to sand. Van recoverable, Tobago beyond it. |
1 Attachment(s)
Originally Posted by Pinky the pilot
(Post 11143922)
Doesn't that cause, amongst a few other things, to make both the fuel dump and the chemtrail dump valves jam open?:confused:
Simply, the modern replacements are not up to the standard of the original General Electric versions. I've attached a data sheet which highlights the high quality units that we once enjoyed. Sadly, not everything new is better. |
"According to the ABC, this is a five seat military trainer. I'm sure Geoffrey Thomas will be able to tell us exactly what happened, though I suspect a faulty flux capacitor." |
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