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-   -   engine failure, how common? (https://www.pprune.org/pacific-general-aviation-questions/345952-engine-failure-how-common.html)

butterfingers 6th Oct 2008 12:05

engine failure, how common?
 
Hi all

I've been flying for about eight years without incident, however i've just had my second engine failure in 12 months. 2 different aircraft, 2 different operators, 2 different maintenance organisations. Both times I was able to restart the engine and land safely.

Obviously I dont want to become complacent and think 'it wont happen to me again'. But I am wondering how many engine failures people have in their careers. Am I due for more? or is this it for a while?

Cheers

BF

Jabawocky 6th Oct 2008 12:10


Both times I was able to restart the engine and land safely.
:hmm::rolleyes:

and a name like BUTTER FINGERS :}

I would suggest you see your local school and LAME about fuel valve management :}

I hope your run of misfortune is able to be circumvented in future!

J:ok:

ForkTailedDrKiller 6th Oct 2008 12:19

Just curious ............. but, what sort of engine failure(s) allows you to restart the engine?

Mechanical fuel pump failure?

Dr :8

troppo 6th Oct 2008 12:31

Three views. Three replies. The previous two should just about cover it.

Horatio Leafblower 6th Oct 2008 12:39

Three engine failures in 3,500 hours - one a fuel system blockage in a Thruster (two-stroke ultralight deathtrap), one a broken exhaust valve rocker on a Cessna 150, and the last one (hopefully) a perished oil-seal at the back of a TIO-540 on a Cheap-tin.

:ouch:

Moved away from the bottom-end of GA operations after that :}

ForkTailedDrKiller 6th Oct 2008 13:11

I have had 3 partials only - in a couple of thousand hours!

1) A run-in with carby icing in a PA28, way back - uneventful restoration of noise
2) Core fell out of a spark-plug in a PA38 and got chewed up in one pot, just after turning X-wind on climbout with a student pilot flying - uneventful return to rwy.
3) Turbocharger on a C402B crapped itself on TO from Rwy 01 YBTL with a full load of punters during the airline pilots strike - big spike in my heart rate and tear-drop turn over water for a return onto Rwy 19 - fire engines and the whole deal!

I have just clocked 600 hrs in the FTDK - 88,000 nm = 4 x round the world - hasn't missed a beat!

Dr :8

butterfingers 6th Oct 2008 13:29

Thanks for your input fellas. Yeah Jaba, I know the name is a bit suss for a topic such as this!

Anyway, last years failure, more so a partial failure, was due to carby ice (my fault, I know).
Todays glitch, after getting checked out by a LAME has been put down to a fold in the tank bladder cutting off the fuel outlet.

ForkTailedDrKiller 6th Oct 2008 13:34


last years failure, more so a partial failure, was due to carby ice
Todays glitch, after getting checked out by a LAME has been put down to a fold in the tank bladder cutting off the fuel outlet
Neither of which were a failure of the engine!:E

Dr :8

Green gorilla 6th Oct 2008 13:41

Been flying for twenty years in around 20 different aircraft without a problem call it LUCK.

butterfingers 6th Oct 2008 13:43

Neither of which were a failure of the engine!http://static.pprune.org/images/smilies/evil.gif

Ok,Ok, I get your point Doc. Still, the fan out front wasnt making a noise!
Well, not a nice noise! :}

the wizard of auz 6th Oct 2008 17:26

A partial in a C150 at about 30Hrs. (Valve)
A partial in a C150 at about 300Hrs( fuel contamination)
A complete in a P68B at about 500Hrs(Acc drive gear)
A complete in a C172 at about 4500Hrs(Carby butterfly shaft breakage)
A Precautionary shut down in a C310 at 4600Hrs (oil termp indication)
A partial in a C172 at around 5000Hrs (Valve and then piston failure)
Otherwise I'm doing alright at around 8500ish. :eek:
Haven't managed to bend one yet.

Capt Claret 6th Oct 2008 23:37

13,000 hours or thereabouts, over 25 years.

1 unscheduled auto feather in a DH8-200 (water in a PFM box)
1 faulty overspeed governor shut down #3 (ALF502) just after take off.

300Series 7th Oct 2008 00:12

In 700Hrs

3 x Partial Engine Failures (still had enough power to make a safe landing) (1 was overwater outside gliding distance)
4 x Electrical/Alternator failures
2 x Undercarriage not come down (1 was hydraulic actuator failure in C72R the other was nose gear overtravel in a baron due to faulty brake motor in the system causing the nosegear to overtravel and jam up) managed to get the baron's wheels down manually on the last attempt. Landed the Gutlass with wheels unlocked at night.

300

bilbert 7th Oct 2008 00:39

10'500 hrs mostly GA - expecting my 9th engine failure any day now.

4Greens 7th Oct 2008 01:25

Apart from a couple of hundred hours in pistons for military training, I had ten years mil flying followed by thirty years airline. Never had an engine failure. Not luck just better and more reliable equipment.

tinpis 7th Oct 2008 01:41

Things better today than they were 50 years ago
It was take a cut lunch and yer water bottle to work then :ooh:

02JUL37 US Export CofA E-2870 issued.
04JUL37 Completed at Lockheed, Burbank as L-10B with Wright Whirlwind engines.
09AUG37 Arrived at Victoria Dock, Melbourne as deck cargo on the S.S. "Mirrabooka" on delivery to Ansett Airways.
13AUG37 Registration application from Ansett Airways Ltd.
16AUG37 Test flown at Essendon.
26AUG37 Added to the Australian Register as VH-UZO. On the same day, the aeroplane was test flown by Lockheed test pilot, Moyle Stephens who gave dual instruction to Ansett pilots including R.M. Ansett.
30AUG37 First survey flight Melbourne-Mildura-Broken Hill by Captains V. Cerche and H.F. Boston.
MAR42 Participated in the evacuation of Broome, WA and Darwin NT after Japanese air raids.
JUN42 Leased to the USAAF for 3 years. Operated mainly Melbourne-Cairns and Melbourne-Darwin averaging 20 hours daily.
12SEP42 Forced landing near Seymour, VIC due propeller failure.
05OCT42 Taxied into a refuelling unit at Townsville and damaged.
OCT42 Based at Mascot, Sydney on USASOS charter Sydney-Townsville.
12OCT42 Forced landing at Rockhampton, QLD due oil leak.
17OCT42 Forced landing at Rockhampton, QLD due oil problems.
18OCT42 Two forced landings at Rockhampton due oil problems. Engine changed.
21NOV42 Forced landing at Archerfield, QLD due to engine failure.
06FEB43 Forced landing at Old Bar, NSW due oil pressure.
09FEB43 Forced landing at Townsville due oil pressure.
07MAR43 Severely damaged during wheels up forced landing at Somerset Dam near Brisbane, QLD. Prop blade broke off in flight and engine broke loose from mounts.
30MAR43 Aircraft en route to Essendon by sea.
29JUN43 CofA renewed after test flight at Essendon after major rebuild.
09JUL43 Forced landing at Mascot due rough running engine.
12JUL43 Struck refuelling unit at Townsville damaging propeller.
13AUG43 Forced landing at Rockhampton due rough running engine.
21AUG43 Forced landing at Mascot due rough running engine.
22NOV43 Forced landing at Mascot due rev drop on starboard engine.
17DEC43 Forced landing at Townsville due engine trouble.
20DEC43 Forced landing at Mascot due oil pressure.
27JAN44 Forced landing at Archerfield due oil pressure.
30JAN44 Forced landing at Mascot due fuel pressure.
06MAR44 Forced landing at Casino, NSW due engine failure.
09APR44 Forced landing at Archerfield due instrument failure.
10APR44 Forced landing at Archerfield due engine trouble.
20APR44 Forced landing at Rockhampton due engine trouble.
23APR44 Forced landing at Rockhampton due engine trouble.
27OCT44 Trailing HF aerial struck by lightning while on charter flight Sydney-Melbourne-Sydney. Explosion inside the cabin opened the escape hatch. Forced landing at Holbrook, NSW.
04NOV44 Forced landing Rockhampton, returned after departure due rough running starboard engine. Landed at 1411 local. Cpt. Charles Gatenby, F/O Charles Eather.
05NOV44 Forced landing Coffs Harbour due rough running starboard engine. Given ground run then continued flight to Sydney but subsequently force landed at Kempsey with similar problem. The spark plugs in the starboard engine were cleaned and the engine ground run. Cpt. Charles Gatenby, F/O Charles Eather.
08NOV44 Forced landing at Woy Woy, NSW due noise on cabin roof. Found to be rubber packing from cockpit escape hatch.
14NOV44 Forced landing at Mascot due rough running starboard engine.
28NOV44 Forced landing at Mascot due oil pressure in port engine.
03DEC44 Forced landing at Mangalore, VIC due engine trouble.
14DEC44 Badly damaged in forced landing near Tumut, NSW. Trucked to Essendon for repairs.
07APR45 CofA renewed after test flight at Essendon.
01SEP45 An overnight wind storm at Parafield blew Lodestar VHCAC into VH-UZO damaging a wing of VH-UZO. VHCAC had been parked with brakes on but no chocks. (NAA via G. Goodall)
45 Returned to commercial service with Ansett Airways.
24AUG49 CofA expired and not renewed.
01MAR50 CofA renewed until 03MAR50 to allow test flights at Essendon prior to sale.
01MAR50 VH-UZO was demonstrated to Adastra at Essendon. Adastra were considering purchasing the aircraft from Ansett Airways but a sale did not eventuate.
05JAN51 Sold to South Coast Airways Pty Ltd, Wollongong, NSW as VH-UZO. To be used on services between Sydney and Cowra.
03FEB51 CofA renewed.
15MAR51 Undercarriage collapsed prior takeoff at Wollongong.
11MAY51 Test flown after repairs and CofA renewed.
07AUG53 Sold to Christey's Motors Pty Ltd, Sydney as VH-CMA.
05DEC55 Sold to Carsair Air Service (PNG) Pty Ltd.
15OCT58 Sold to Western Air Navigation Pty Ltd, Charleville QLD as VH-WAO.
27JUL60 Sold to C.H. Degotardi Air Services Pty Ltd, Sydney as VH-CHD. Based at Bankstown, Sydney and used mainly to fly potential customers to inspect real estate. Named "Miss Real Estate".
06DEC62 Sold to Marshall Airways Pty Ltd, Bankstown, NSW as VH-ASM. Used for general charter and aerial ambulance work.
23JUL67 Emergency landing at Bankstown with smoking engine and suspect undercarriage. Believed to be last flight for Marshall Airways.
27OCT67 Struck off Register as withdrawn from use.


VH-UZO - The Lockheed File

Howard Hughes 7th Oct 2008 04:17

Doing a quick straw poll among friends I reckon it's around once every 6000 hours! As 4 Greens says the better equipment you fly, the better off you are! Most people I know have had failures in pistons, although I do know of two total failures in turbines, one was a fuel pump and the other reduction gears...:ooh:

Jet's of course fail everytime you get in the sim!;)

Contrary to popular training practices, not many failures happen on take off!:rolleyes:

bushy 7th Oct 2008 05:45

two in 15,000 hours GA
 
I had two turbo charger failures in a chieftain on climbout. Otherwise no engine failures in 15,000 hours in GA.

Ultralights 7th Oct 2008 05:59

700 hrs in Jabiru's and GA, only 1 failure, throttle stop bracket on carby broke, allowing throttle to go to idle/cutoff when turning final. in a Jab LSA

TexanPilot 7th Oct 2008 06:59

3500 hours I have had... 2 x partials, 1 full failure (Magneto failure), numerous gear failures (always able to manually extend), numerous electrical failures, 1 precautionary shutdown of a turbine and 1 engine fire in flight.

ahhh the good old days :}


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