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Lucky Escape - VH-EXA PA30 Crash on take-off in Ferry Configuration

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Lucky Escape - VH-EXA PA30 Crash on take-off in Ferry Configuration

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Old 28th Jun 2012, 09:13
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Lucky Escape - VH-EXA PA30 Crash on take-off in Ferry Configuration

Here's another serious accident that seems to have escaped notice on this forum. The aircraft was fully fuelled for the 2200 NM ferry flight from Hollister to Hilo, and suffered a power loss just after lift-off. Gary Mitchell, a very experienced ferry pilot escaped the inverted wreckage without injury.

Here is the NTSB summary reported on Aircraft Owners - Airplane Owners and Registration Data Ferry Accident

In preparation for an extended over-water ferry flight, a ferry fuel tank system was installed on the airplane. On the day prior to the accident a certificated airframe and powerplant mechanic inspected the ferry fuel system, finding the airplane airworthy with respect to the work performed. The pilot then conducted a successful test flight of the ferry fuel system, with no anomalies noted. Prior to takeoff on the accident flight the pilot ran both engines up to full takeoff power, followed by brake release, after noting that takeoff power had been achieved. After the airplane became airborne the pilot selected the gear selector switch to retract the landing gear, with all indications normal. He reported that, when the airplane was about 60 feet above the ground, there was a loud bang and that the left engine subsequently “surged” and lost partial power. A witness stated that after the takeoff he heard a loud popping noise, and the pilot stated that the nose pitched up and he intuitively pushed forward on the yoke. The pilot reported that the engine power eventually returned; however, not before the airplane impacted terrain and came to rest in an inverted position. A postaccident examination of the airplane and engines failed to reveal the reason for the reported partial loss of engine power.
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