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Old 12th June 2016 | 06:15
  #22 (permalink)  
Marchettiman
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Joined: Mar 2006
Posts: 110
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From: 52N
Power is supplied to the landing gear actuator by two solenoids, one for each direction of movement. It's my bet that the "up" solenoid has failed in the closed sense so it is continually supplying 28v to the actuator. You can test that by checking that there is no voltage being supplied to the solenoid when the aircraft on the ground with the weight on the main wheels so the squat switch is closed.
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