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Old 18th Feb 2011, 04:44
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DERG
 
Join Date: Oct 2009
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Swarf in the oil

I have seen a report where one of the Qantas T972s had metal chips on the magnet trap SEE BELOW Glad OE has posted!

This is the type of metal trap we are talking about
Vibro-Meter Magnetic Chip Detectors and Chip Collectors

In fact the 900 series is the first to have a chip detector that sends messages back to base. It is detailed, along with the other sensors on the engine here..
http://www.ingenia.org.uk/ingenia/is...e39/Waters.pdf

and moreover
Ingenia Articles

Qantas A380 engine had problems before explosion
6.12.2010 (Sydney Morning Herald)

It's been revealed that the engine that disintegrated on a Qantas Airbus A380 near Singapore last month had earlier been taken off the aircraft to fix another problem.

The Australian newspaper says investigators have revealed that the engine was only refitted in February.

An Australian Transport Safety Bureau report released last week shows the No 2 engine was originally fitted as the aircraft's No 4 engine but was removed last year after metal was found in a chip detector.

Chip detectors are often a permanent magnet used to gather metal fragments, usually from lubrication oil.

The relatively new engine had performed just 3419 flight hours and 416 landing and take-off cycles at the time.

The engine was sent to a Singapore workshop certified to maintain and repair Rolls-Royce engines in September last year.

Engineers found spalling in a low-pressure compressor bearing and replaced the bearing assembly. Spalling occurs when flakes break off from a larger component and is usually associated in mechanical systems with high-stress points.

The low-pressure compressor is a different part of the engine than the one that failed in the dramatic Singapore incident.

The repair was completed in December last year. The engine was fitted to the aircraft on February 24 and had completed a further 2895 flights.

Last edited by DERG; 18th Feb 2011 at 05:45.
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