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Old 5th Sep 2010, 10:56
  #217 (permalink)  
M2dude
 
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Devil In-Flight Reverse (A case of Bucket and See)

Capt Chambo
Concorde was, as EXWOK says, could use reverse in flight, on the inboard engines only, and only as far as reverse idle, the mechanism of which was quite complex and did on occasion not do work as advertised. Bear in mind here that the Rolls Royce Olympus 593 was a pure turbojet with no bypass, and so a hot stream reverser only had to be used; the reverser buckets acting directly on the efflux as it did any reverser in the 'old' days. Also the same buckets that were used for reverse were also progressively opened up between Mach 0.55 and wide open at Mach 1.1, this giving a vital control enhancement to the divergencing efflux. The overall effect of this was to give a true overall convergent/divergent nozzle assembly, the ideal for any supersonic aircraft.
As far as inflight reverse goes, the amount of HP compressor delivery air (P3) required to actuate the bucket airmotor in flight at an idle thrust settings, was quite minimal to say the least, and some help was definitely needed here. The moment that inflight reverse was selected (on the inboard engines only remember) the OUTBOARD engines would have their idle N2 automatically increased, and some of THEIR P3 air supply was also automatically ported over (via an isolation valve) to the inboard buckets. This whole process was required in order to give a little added muscle to the bucket airmotors, and give the system a fighting chance. Even this however was still not quite enough, the inboard travelling buckets required minimal air loading on their surface, and so the primary nozzles for the affected engines (the primary nozzle lived just aft of the LP turbine, aft of the reheat assembly) was automatically signalled wide open in order to assist matters here, by reducing gas velocity. One the buckets had reached full reverse the primary nozzle was then signalled full close (this applied for normal ground reverse also) and the automatic increased idle on the outboard engines was cancelled. To enable the described process to occur, provided all four engines were at idle, a solenoid latched button on the F/E's station could be selected. This signalled a circuit that enabled the selection of idle reverse on the inboard engines only, the opening of the P3 isolation valve, the raising of the outboard engine's idle and maximum primary nozzle angle for the outboards as soon as reverse was then selected..
The whole system was just a little fragile here; failure of either the extra air supply, or the raised idle on the 'other' engine was usually enough to stop the process working correctly.
EXWOK
While flying 'up front' I only ever experienced the use of inflight reverse once. (The captain was a bit of an Animal, if you flying guys see what I mean ). I would not say that it felt as if we'd hit a brick wall, as I'd expected the sensation to feel, more like we were flying into the dumped contents of a very large manure truck . The whole operation was so slick, we'd dumped the required amount of IAS more or less within a second or two, and normal thrust was immediately selected. As so often happened with you guys, you made it look too easy.
As far as the speed of the airmotor goes, I seem to remember that it was something in the order of 80,000 RPM at max chat; as you say faster (around twice as fast) as the standby horizon motor.
The basic core airmotor (not the whole assembly) was the same Garrett unit used on the P&W JT9 as well as the RB-211.

Dude

Last edited by M2dude; 5th Sep 2010 at 12:25.
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