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Old 11th Feb 2009, 11:55
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Leeuwarden AFB-Ed
 
Join Date: Feb 2009
Location: Leeuwarden
Age: 59
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testresults pitch link change

What we did too reduce the feedback load from the rotor to the collective system is:
Lenghten all four pitch links with two full turns followed by the 100% full hydr.test during ground run.(we're not going to fly)
Up to 92% rrpm it is possible to bottum the collective with only one hydr.sys.so it defenitly has to do with the rotorsystem. With 100% rrpm its about 10-15 mm from full down with a small difference between the hydr.systems.
We're gone change a set rotor blades and hopefully this will work out.
Leeuwarden AFB-Ed is offline