PPRuNe Forums - View Single Post - AAIB initial report out on BA B777 crash at LHR
Old 20th Jan 2008, 20:04
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Riverman
 
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GMDS
Granted the following AD applied to GE90's but does appear to confirm that there are paths where FADEC signals can be corrupted.



SUPPLEMENTARY INFORMATION: The Federal Aviation Administration (FAA) has received seven reports of loss of thrust control (LOTC) on General Electric Company (GE) Model GE90 turbofan engines installed on Boeing 777 series aircraft. Five LOTC events occurred in-flight and two occurred on the ground. The five in-flight LOTC events were temporary in that the engine recovered and continued to operate normally for the remainder of the flight.

Investigation

The investigation revealed that water can accumulate in the Ps3 and P3B pressure sensing system, which can freeze in the full authority digital engine control (FADEC) sensing ports or pressure line. Frozen water can result in a restriction or a blocked signal to the FADEC. This blocked signal can cause a corruption of the FADEC signal and result in abnormal engine start characteristics on the ground or lack of engine response to commanded thrust levels in flight. Although there have been no LOTC events attributed to icing of the P3B sensing system in the field, inspections have identified moisture in this system, which could freeze and corrupt the P3B signal to the FADEC as well. This condition, if not corrected, could result in LOTC due to blockage of the FADEC sense lines, which if it occurs in a critical phase of flight, could result in loss of aircraft control.

Simultaneous LOTC Events

The FAA is especially concerned about the possibility of simultaneous LOTC events on both engines installed on the Boeing 777 series aircraft due to common mode threats, such as certain atmospheric conditions that may result in ice in the Ps3 or P3B pressure sensing system and causing corrupted signals to the FADEC in both engines.

SUMMARY: This amendment adopts a new airworthiness directive (AD) that is applicable to certain General Electric Company GE90 series turbofan engines. This action requires visually inspecting Ps3 and P3B sense lines and full authority digital engine control (FADEC) Ps3 and P3B sensing ports and fittings, cleaning Ps3 and P3B fittings and sensing ports, purging the Ps3 and P3B systems of moisture, and, if necessary, blending of high metal, nicks, burrs, or scratches on Ps3 and P3B fitting threads. This amendment is prompted by seven reports of loss of thrust control due to corruption of the signals to the FADEC caused by water freezing in the Ps3 sensing system. The actions specified in this AD are intended to prevent loss of thrust control due to corruption of the Ps3 and P3B signals to the FADEC which if it occurs in a critical phase of flight, could result in loss of aircraft control.

Interim Action

Both Ps3 and P3B pressure systems incorporate weep holes that allows drainage of water in the lines that may accumulate from condensation or ingested water; however, the field events and the investigation have determined that these design features may not always be effective in eliminating water from these systems. GE is assessing design changes that will prevent water from freezing in these systems and causing corruption of the signals to the FADEC. The requirements of this AD may change based on the ongoing investigation of the root cause and field inspection results, and future rulemaking may be necessary.
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