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Old 1st May 2019, 20:01
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Smythe
 
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The LEAP engines are both larger and relocated slightly up and forward from the previous NG CFM56-7 engines to accommodate their larger fan diameter.
This new location and size of the nacelle cause the vortex flow off the nacelle body to produce lift at high AoA; as the nacelle is ahead of the CofG this lift causes a slight pitch-up effect (ie a reducing stick force) which could lead the pilot to further increase the back pressure on the yoke and send the aircraft closer towards the stall.

This non-linear/reducing stick force is not allowable under FAR §25.173 "Static longitudinal stability".

Several aerodynamic solutions were introduced such as revising the leading edge stall strip and modifying the leading edge vortilons but they were insufficient to pass regulation. MCAS was therefore introduced to give an automatic nose down stabilizer input during elevated AoA when flaps are up.​​​​​​​"
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