PDA

View Full Version : Plane crashes on overrun in eastern Georgia, USA


fotoguzzi
21st Feb 2013, 05:39
"The Hawker Beechcraft 390/Premier I crashed around 8:30 p.m. at the Thomson-McDuffie County Airport, about 30 miles west of Augusta, Federal Aviation Administration spokeswoman Kathleen Bergen said in an email."

This was the flight's destination, so it seems safe to presume that the overrun occurred on landing.

5 Dead After Small Jet Crashes in Eastern GA - ABC News (http://abcnews.go.com/US/wireStory/small-jet-aboard-crashes-eastern-georgia-18553040)

METAR KHQU 210055Z AUTO 00000KT 10SM CLR 09/M04 A3012 RMK AO1 T00931044 =

This link has tail numbers and personal names. As far as I can tell, none of this information has been officially released:

Thomson jet crash kills 5; 2 survivors hospitalized | The Augusta Chronicle (http://chronicle.augusta.com/news/2013-02-20/plane-crashes-near-thomson-airport?v=1361418398)

sevenstrokeroll
21st Feb 2013, 09:53
thank you for posting this and esp for the metar.

I'll have to look at the runway information, esp slope of runway *(if any).

Calm and clear...ouch.

sevenstrokeroll
21st Feb 2013, 10:18
http://webcache.googleusercontent.com/search?q=cache:3F5lyDq0Lc4J:http://www.airnav.com/airport/KHQU+KHQU&hl=en&ct=clnk

the above has info on the airfield.

ILS to runway 10. PAPI both ends of runway. 3 degree GS.

of interest, warning of deer on runway at night (in general).

about 5200feet long, 100 feet wide

runway 10 slopes UP.

unsure of landing direction of aircraft.

may have been pilot activated HIRL

fotoguzzi
21st Feb 2013, 12:47
[Later: early consensus seems to be that it IS a Runway 10 overrun that somehow missed the manufacturing plant and motored along until it encountered a forest.]

I am not entirely convinced that this is an overrun event:

"Mike Miller, reporting: 'Now, I want to give you an idea of where this plane actually crashed at. We are standing alongside Washington Road right now, and to my right, across the street, behind those buildings...that is where the airport is. Now, back over here to my left, is where the Milliken Plant is. You probably can't see it because it's dark, but a mile and half behind the plant, that's where deputies say the plane crashed at.'"

From civilian online mapping, Washington Road is at the threshold to Runway 28 and would be the first thing encountered if Runway 10 were overrun. Milliken Plant is the next thing encountered and could just be avoided in a Runway 10 overrun. Then go another mile and a half....

A mile and a half past the end of the runway seems to me a long way for a plane to hold together. It would be easier for me to believe that the plane hit short of the threshold to Runway 28.

DEVELOPING ON 6: New Information Released In Deadly McDuffie County Plane Crash Investigation | ABC 6 WJBF-TV (http://www2.wjbf.com/news/2013/feb/21/5/developing-6-500-m-update-deadly-mcduffie-county-p-ar-5643795/)

sevenstrokeroll
21st Feb 2013, 14:14
you make some fine points!

having an ILS is a plus at night (10)

and not having an ILS allows for many visual deceptions, esp with a downslope on runway 28...even with a papi (assuming facts not in evidence)

clear and calm...wondering what calm wind runway was/is.

and without knowing more, I would think that coming from nashville tenn would set you up for runway 10 on a semi straight in.

oh well...be careful out there.

I sort of thought they saw some deer at the last second and tried to hop over them and came down really long.

sevenstrokeroll
21st Feb 2013, 18:33
I saw a graphic of the course flown by the jet...it seems to me the guy was flying as direct as possible to the airport, entering a modified base leg perhaps too close to the field to get stablized on the approach.

Even one statement by another pilot that the pilot in question ''flew fast'' and some of us know what that means.

high, fast, out of position...maybe pushed it on to the runway and couldn't stop...maybe even tried to go around and stalled her in...ouch

robbreid
21st Feb 2013, 21:07
Hearing it was an aborted landing, aircraft struck a 60' utility pole and crashed into the trees and fragmented.

There was a NTSB Press meeting at 13:30 EST today - should be a press release soon.

robbreid
21st Feb 2013, 21:21
Aircraft aborted landing runway 10 for unknown reasons, it's port wing struck near the top of a 60' concrete utility pole approx 1/4 mile from end of rw 10 - severing the left wing, the airplane continued for another 1/4 mile (1/2 mile from end of runway 10) impacting trees - crash site reported as 100 yards long completely destroying (fragmenting) the aircraft.

NTSB briefing; Member Robert Sumwalt briefs the media on Thomson, Ga. aviation accident, February 21, 2013. - YouTube (http://www.youtube.com/watch?v=az5VUq3r4dU&feature=youtu.be)

sevenstrokeroll
21st Feb 2013, 22:07
I heard that also. ON an aborted landing (I read go around) they hit this pole and sheared off the left wing.

wow.

it almost always takes less time to do it right the first time...that means: stable apch = good safe landing.

robbreid
21st Feb 2013, 23:32
So 1/4 mile from end of runway 10 the aircraft was flying at less than 60 feet agl!!!

Full 16 minute NTSB briefing from crash site; https://twitter.com/bizjet101/status/304716032256385025

Aircraft was equipped with a L3 FA2100 CVR.

robbreid
22nd Feb 2013, 01:41
FOR IMMEDIATE RELEASE (from The Vein Guys, N777GV Owners)

Evans, Georgia, February 21, 2013 - Last night, February 20, 2013 at approximately 8:30 p.m. a plane carrying Vein Guys employees was involved in an accident at the Thomson-McDuffie County Airport after a routine trip returning from Nashville, Tennessee.

The company is still working through the details of the events that transpired leading up to the incident and as additional information becomes available they will release it to the public as appropriate.

As of today, confirmed information is that both pilots survived the crash and are being treated at MCG Hospital in Augusta. It is with deep sadness that we report that five members of our staff on the plane were killed in the accident, including our Chief Physician, Dr. Steven Roth. We send our deepest condolences to the families of the individuals who were lost.

“We are a family and our hearts weigh heavy today as we have lost members of our team- words cannot express our grief,” said Kelly Vann, Chief Operating Officer of the Vein Guys.

Out of respect for the families, the names of the deceased will not be released at this time.

fotoguzzi
22nd Feb 2013, 08:43
Thank you, robbried. Not much to add except that civilian mapping sites, the press conference, and a news photograph give me the impression that the pole struck was perfectly aligned with Runway 10 as was the area where the debris has concentrated. The plane traveled directly over the corner of the manufacturing plant but was obviously unable to clear the 60-foot tall pole that was just behind the plant. By passing to the right of the pole, there was little chance to avoid hitting the wires.

DownIn3Green
22nd Feb 2013, 20:11
OK, all of this is great talk...only one poster seems to ask the obvivous question...1/4 mile past the departure end of rwy 10, the guy was still only at 60'?

Either a catostrophic failure, weather related issue (being generous here) or simply a cocked up approach and "go-(almost) around...

Why can't people here wait for the facts and accept the fact that some accidents may be "pilot error"?

His dudeness
23rd Feb 2013, 08:47
Why can't people here wait for the facts and accept the fact that some accidents may be "pilot error"?

Has pilot error being ruled out yet? If so, by whom?

ksjc
23rd Feb 2013, 13:49
I too wonder how they were at only 60' well beyond the end of the runway but 1/4 mile is 1300' which isn't really that far. If it was one of those jobs where the pilot tried to get airborne again because he thought he was running out of runway he could have been very low trying to get his speed up and cleaned up. These don't always turn out too well.

Off the top of my head I can think of an HS-125 in Minnesota and a Citation in Carslbad, CA within the past few years trying the same thing and both turning into disaster. I'm sure there are many others.

galaxy flyer
23rd Feb 2013, 16:20
Small note, runway 10 has a 1% UP gradient, assuming the terrain continues rising, 60' above the terrain might be 75'-80' above DER elevation of 10 and perhaps 120' above the touchdown elevation of runway 10.

GF

robbreid
23rd Feb 2013, 23:38
On a positive note, the Captain Richard Trammell who was found strapped in his seat in the remains of the cockpit, has been upgraded from 'Critical' to 'Fair' and is receiving visitors and talking coherently.

The Co-pilot Jeremy Hayden was found walking 300 feet away from the wreckage, his condition has not been released but was said to be the lessor injured.

Also NTSB has 5 witnesses along with a grainy CCTV video, also runway was searched and nothing out of the ordinary was found.

sevenstrokeroll
24th Feb 2013, 19:27
down in three green

for the longest time I tried to find a non pilot reason for accidents...I really mean it. Trying to blame many things other than pilot screwup.

Well, this one sort of looks like that. Just a screw up...maybe not a long enough final to be stable, maybe not awareness of the terrain features near by...maybe letting the copilot fly a tough approach when it should belong to the captain.

maybe night vision problems....get there itis.

yup...maybe its better to start with pilot error and then look around for other things.

and why wasn't the post/pole illuminated???

sevenstrokeroll
25th Feb 2013, 20:22
just read that the composite structure was pretty much completely destroyed.

wondering if a metal plane would have offered more survivors.

fotoguzzi
25th Feb 2013, 22:51
sevenstrokeroll: My civilian impression based on the initial press briefing and aerial and news photographs makes me understand that the wires had three orange balls on them. I'm not sure if a sixty-foot pole perfectly aligned with the runway should have a light or not.

Again my impression of the scene is pieced together and may be inaccurate.

galaxy flyer
26th Feb 2013, 01:07
Sometimes, a plane cannot avoid the illuminated aerial or tower--physics is a real arbiter.

GF

DownIn3Green
26th Feb 2013, 01:24
Seven,

I am the first guy in line to try to find why the guy upfront didn't screw up...but sometimes you are unnfortunately correct, and as I alluded to as well...

Assume an unstablized approach from which a go-around was initiated...

Several things come to mind:...An engine failure...a bird strike on the windscreen startling the crew...a Primary Flight Control failure (at an unopportune time...Electrical failure resulting in the Primary Flt Instruments and cockpit lights going out...Some sort of structural failure...passenger interference...the list could go on and on...

However, the examples above are far less likely to occur than a simple pilot error resulting in this terrible tragedy...

I am a fan of Robert Serling, the great aviation writer...He wrote a book titled "The Left Seat", which was fiction but loosly based around any one of the "Big Four" in the 40's through the Jet Age...

The Story centered around the fictional McDonald MacKay, from his "new hire class" through his Captaincy of his airline "Midwest" (substitute Eastern, American or United). As a DC-7 Captain, this ALPA Safety Committee Chairman crashed his DC-7 on evening at Idlewild (JFK) during a missed approach, and in the aftermath realized it was he who screwed up...

A tear-jerker, but he fessed up and everything turned out ok in the end...

My point is, while everyone else was looking to exonerate him, he realized that pilots, even excellent ones, can have a bad day...It cost our fictional hero...but that was fiction...

Some time fiction is not only stranger than truth...it sometimes parallels it...

galaxy flyer
26th Feb 2013, 01:48
Both the Carlsbad and Ottumwa, MN crashes occurred because the pilots asked more of the plane than it could deliver, might (MIGHT) be the same here. Long landing, late go-around decision, physics takes over!

GF

westhawk
26th Feb 2013, 04:02
IIRC, in the Carlsbad crash the approach was flown at such an excessive speed that landing and stopping on the runway surface was impossible. A very late go-around was attempted, but far too late to avoid hitting the LOC antenna array.

In the Hawker crash in Ottumwa, the speed was within normal approach speed range for the conditions, but with a tailwind component and a slightly long landing within the TDZ. On a wet runway, braking was ineffective and a very late go-around was attempted resulting in the airplane leaving the ground after the runway end. The crew coordination was less than ideal, resulting in the flaps being selected up prematurely. This ultimately led to an asymmetric stall and collision with the ground. Reading the report and CVR transcript, it was never clear to me that lift dump was ever fully deployed, perhaps contributing to the lack of braking effectiveness. Had the PIC elected to continue the stop instead of aborting the landing, it very likely would have been a low speed runway overrun event rather than a fatal crash. At some point in every landing, committing to stay on the ground and discarding any thought of a go-around must occur. In the Hawker, selection of lift dump is normally considered to be the act which commits you to staying on the ground, as much as T/R selection does in other aircraft.

What do these two accidents have in common with the Premier crash in Georgia?

NTSB board member Mark Rosenker is quoted as saying in a briefing last week (according to Avweb.com (http://www.avweb.com/avwebflash/news/ntsb_pilot_georgia_premier_jet_crash_fire_abort_208213-1.html) and available for viewing at NTSB.gov (http://www.ntsb.gov/)) that the airplane had clipped a utility pole and crashed following an aborted landing.

I seem to recall a spate of overruns in the Premier 1 when it first entered service a few years ago. Something to do with the lift dump system and supposedly addressed by Raytheon/Beech.

So it seems quite possible that this accident has a couple of things in common with one or both of the above cited accidents. Thanks ksjc and GF for mentioning them. Since the NTSB was having a slow week and saw fit to send a major investigation go-team to the crash, (not normal for non air carrier accidents not involving well known celebrities) it seems likely that information on this accident will be more visible for internet accident investigators like me via the NTSB website.

westhawk

sevenstrokeroll
26th Feb 2013, 11:58
three green...I read "the left seat" many years ago too. serling (the non twilight zone brother ) was great...didyou ever read, 'wings"...it was a fictionalized story of aleghany airlines (now usairsoontobeamerican).

great books...imagine real books with real paper!!!!

anyway, your examples are good...engine failure on go around, flight control failure, instrument failure...but a pilot should be ready for an engine failure at any time, same with the rest...shifting modes in you rmind right away.

yes, its tough to have a control failure at sixty feet and get away with it...but

anyway, maybe it was something else...who knows, maybe a passenger went nuts and used a scalpel to knife the pilots on short final...but Idont' think so.

premiere has lift dump? hmmmm, I flew the handle page with lift dump...very effective...but we did have one guy who had lift dump deploy on final prior to landing.

serling...great books

did you ever read "the crowded sky", not by serling...just the cover review was fascinating.

galaxy flyer
26th Feb 2013, 15:48
Westhawk

I my humble view, the, perhaps, no report yet, common thread is late or incorrect decisions to try and get airborne again.

GF

DownIn3Green
26th Feb 2013, 22:08
Seven Stroke...thank you for the kind reply...

No I never read "Wings", but I've had a few friends from Allegheny (and Piedmont) in the past...I'll have to try to find it...Serling never wrote a bad aviation story, fictional or non-fiction...(The Electra Story) comes to mind...

Have you ever read "She'll Never Get Off The Ground"?...Fiction but loosely based on the USA's first Female Airline Pilot...Dudney Devlin was the pilot in the book, but it was (I forget her name) who broke the "barrier with Frontier in the 70's...

As for "The Crowded Sky", no never read that one, but I saw the movie...Didn't it have something to do with the flight attendant serving coffee to the cockpit and then one of the guys upfront spilled it on the Auto-Pilot control panel, resulting in a co;;ision with a Military T-33? (flown by Efram Zimbalist Jr).

All lessons us "old, not so bold pilots" learn from...

Maybe the new generation should start paying attention to mistakes we've all made but through the grace of god and our own witts managed to survive, never to repeat again...

galaxy flyer
26th Feb 2013, 22:41
Bonnie Tiburzi, at AA, her dad was around the airport I learned at. Emily Warner was the first at old Frontier, but Bonnie was cited because AA was a "major" in those times.

GF

DownIn3Green
26th Feb 2013, 22:49
GF, Thanks...I'm going to Google that now...Did you read the book? If so, was it an accurate portrayal?...DI3G...










/..

westhawk
26th Feb 2013, 22:59
GF:

Indeed. I once heard it put this way by a friend after we witnessed light single making a very late go-around: "Ya know, I don't think there's much of a future in doin' that very often."

westhawk

sevenstrokeroll
27th Feb 2013, 01:25
three green

''the crowded sky'' a reminder that being on the right altitude matters all the time...no spilling of coffee...that's the movie 'fate is the hunter'.

the book is better than the movie though both are good.

I read many serling books...all of them that I could get as they all had lessons. and my first ride on aplane was the electra...western airlines, the only way to fly.

I think the lessons in books are fascinating and I've learned from all of them.

wings, is very hard to find...maybe a used book sstore. or in this modern world online...I think that's the title.

be well, and always keep those young kids in line!!!!

DownIn3Green
27th Feb 2013, 02:43
Seven...Fate is the Hunter...Ahhh...Captain Ernest K. Gann...wonder how many today who ever heard of him actually know he writes from experience...from among other things his life experiences as an American Airlines Capt...

I googled "Wings" and you're right, it seems hard to find, but I am greatful for the tip...I'd never heard of it, and now I'm determined to read it...

I'm out of the AvBiz now...Thanks anyway, but you keep the techno-geek aviators in line..

bem411s
28th Feb 2013, 20:27
Doesn't this sound just like the Jack Roush crash at Oskosh 2 years ago? Deer on runway + blown go around perhaps? Too simple and too early to speculate but it's the first place my mind went.

CEN10FA443 (http://www.ntsb.gov/aviationquery/brief.aspx?ev_id=20100728X70427)

DownIn3Green
1st Mar 2013, 00:37
And your point being?...

I was offered a job on one of the Roush 727's back in the late 90's...Would have been a Great Job, but I was married at the time and didn't want to move to Charlotte...

Hindsight is 20-20...as was my marriage...

As far as I know Jack Roush runs a pretty good Aviation Department...And I have lots of VIP experience...

bem411s
1st Mar 2013, 01:33
Its not personal, its a very pausible sequence of events which sounds consistent with the scenario. More likely, one might say than some of the other scenarios presented. Around dusk. Deer known to be an issue supposedly. Perhaps didn't commit to the go around or it occurred too late. It should be said i havent seen that this incident involved a stall. That being the primary difference between the two at this point. A few more knots of airspeed and they could be the same.

robbreid
6th Mar 2013, 21:07
NTSB Identification: ERA13MA139
14 CFR Part 91: General Aviation
Accident occurred Wednesday, February 20, 2013 in Thomson, GA
Aircraft: BEECH 390, registration: N777VG
Injuries: 5 Fatal,2 Serious.
This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators traveled in support of this investigation and used data obtained from various sources to prepare this aircraft accident report.
On February 20, 2013, at 2006 eastern standard time, a Beechcraft 390 Premier 1A, N777VG, was destroyed following a collision with a utility pole, trees, and terrain following a go-around at Thomson-McDuffie Regional Airport (HQU), Thomson, Georgia. The airline transport-rated pilot and co-pilot were seriously injured, and five passengers were fatally injured. The airplane was registered to the Pavilion Group LLC and was operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a business flight. Night visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed. The flight originated at John C. Tune Airport (JWN), Nashville, Tennessee, about 1828 central standard time (1928 eastern standard time).

The purpose of the flight was to transport staff members of a vascular surgery practice from Nashville to Thomson, where the airplane was based. According to initial air traffic control information, the pilot checked in with Augusta approach control and reported HQU in sight. About 2003, the pilot cancelled visual flight rules flight-following services and continued toward HQU. The last recorded radar return was observed about 2005, when the airplane was at an indicated altitude of 700 feet above mean sea level and 1/2 mile from the airport. There were no distress calls received from the crew prior to the accident.

Witnesses reported that the airplane appeared to be in position to land when the pilot discontinued the approach and commenced a go-around. The witnesses observed the airplane continue down the runway at a low altitude.

The airplane struck a poured-concrete utility pole and braided wires about 59 feet above ground level. The pole was located about 1/4 mile east the departure end of runway 10. The utility pole was not lighted. During the initial impact with the utility pole, the outboard section of the left wing was severed. The airplane continued another 1/4 mile east before colliding with trees and terrain. A postcrash fire ensued and consumed a majority of the airframe. The engines separated from the fuselage during the impact sequence. On-scene examination of the wreckage revealed that all primary airframe structural components were accounted for at the accident site. The landing gear were found in the down (extended) position, and the flap handle was found in the 10-degree (go-around) position.

An initial inspection of the airport revealed that the pilot-controlled runway lights were operational. An examination of conditions recorded on an airport security camera showed that the runway lights were on the low intensity setting at the time of the accident. The airport did not have a control tower. An inspection of the runway surface did not reveal any unusual tire marks or debris.

Weather conditions at HQU near the time of the accident included calm wind and clear skies.

DownIn3Green
6th Mar 2013, 23:37
BEM411s...

Are you related to our departed friend 411a by any chance?

Any personal feelings aside, but in certain ways I agree with you...However, no stall is mentioned...you are correct...

But a "few extra knots" wouldn't do much for any jet after hitting something that takes a wing off...

bem411s
8th Mar 2013, 14:13
No, I'm not related to anyone else on the board that I know of. my login is just an old one from college years ago I still use some places. Sad situation though. I do have to wonder if both engines were producing power on the go around or if the throttles were retarded for some reason to have such a flat flight path on the go.

galaxy flyer
8th Mar 2013, 15:15
There was a flight aware track posted somewhere showing about 250 KIAS at 5 miles from the runway and 2,500' AGL. I'm wondering if the speedbrakes or spoilers were left extended on the go. Presumably, they auto-retract when the throttles were advanced, but a failure or throttles not being pushed up far enough to retract them. Extended flight and/or ground spoilers (inadvertent touchdown?) would explain the trajectory.

GF

flying mechanik
30th Oct 2014, 08:17
Report is out now.


Sad but true:


The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The pilot's failure to follow airplane flight manual procedures for an antiskid failure in flight and his failure to immediately retract the lift dump after he elected to attempt a go-around on the runway. Contributing to the accident were the pilot's lack of systems knowledge and his fatigue due to acute sleep loss and his ineffective use of time between flights to obtain sleep.


Here the full Report:


ERA13MA139 (http://www.ntsb.gov/aviationquery/brief.aspx?ev_id=20130220X11432&key=1)