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UAL 757 incident at EWR

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UAL 757 incident at EWR

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Old 16th Jun 2019, 07:23
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Originally Posted by Smythe
rear tires flat, front landing gear impaled, reverse thrust still active...that must have been quite the landing....

In related news, United adds another aircraft to their A321XLR order at the Paris airshow.....
Quite the landing ? I think they may have ' arrived '.
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Old 16th Jun 2019, 08:31
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According to meteo reports, the wind was 210/220 13/24 kt, direct headwind.

KEWR 151651Z 21016G24KT 10SM FEW140 SCT180 BKN250 27/09 A3005 RMK AO2 PK WND 20026/1553 SLP177 T02670094
KEWR 151658Z 22013G24KT 10SM FEW130 SCT180 BKN250 27/09 A3005 RMK AO2 T02720089
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Old 16th Jun 2019, 11:12
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Anyone interested in waiting until the investigation is complete and facts are in ?
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Old 16th Jun 2019, 11:22
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I seem to remember Air Europe doing something similar at Funchal? I think it was said that the step down into the flight deck was changed to a step up!

It seems that while the 757 is very easy to de-rotate too quickly, giving a hard nose gear landing, it's not built to take those impacts. My recollection is that if you don't fly the nose gear onto the runway before the autobrake bites, you'll run out of elevator authority and can't prevent the nose slamming in?
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Old 16th Jun 2019, 11:57
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Originally Posted by ZeBedie
I seem to remember Air Europe doing something similar at Funchal? I think it was said that the step down into the flight deck was changed to a step up!

It seems that while the 757 is very easy to de-rotate too quickly, giving a hard nose gear landing, it's not built to take those impacts. My recollection is that if you don't fly the nose gear onto the runway before the autobrake bites, you'll run out of elevator authority and can't prevent the nose slamming in?
Well I’ve only got 4000 hrs on them and you’re talking a fair bit of bollocks there. It’s certainly no harder to de rotate than any other Boeing and certainly easier than certain airbus products. The Air Europe incident was a nose wheel first job in to a notoriously difficult field plagued by wind shear with different winds very often at both ends, where even the local carrier ( presumably fairly exposed to the place ) have pranged a few.
Carrying speed well in excess of Vref greatly enhances the chance of a nose wheel first or shallow touchdown and this looks a classic case of that. As someone said perhaps wait for the actual accident report.
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Old 16th Jun 2019, 12:23
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Originally Posted by Globocnik
Carrying speed well in excess of Vref greatly enhances the chance of a nose wheel first or shallow touchdown and this looks a classic case of that. As someone said perhaps wait for the actual accident report.
Not sure to concur.
Why should people wait for the report in this particular case, while they don't when the accident occurs in another continent with foreing pilots ?
We already do have some facts here : the wind, the state of the airplane.
What we are still to read about, is the usual rigmarole of "should haves", "forgot flying basics", "substandard training", etc.



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Old 16th Jun 2019, 12:46
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Originally Posted by ZeBedie
it's not built to take those impacts.
Are you suggesting that some other aircraft are capable of withstanding a similar impact without suffering structural deformation? What type(s) do you have in mind?
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Old 16th Jun 2019, 13:08
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any compression type buckling on top of the fuselage?
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Old 16th Jun 2019, 13:31
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https://en.wikipedia.org/wiki/Britan...ys_Flight_226A Here, nose wheel 'dog box' failed due over load, resulting in a significant runway excursion.


Final report https://www.fomento.es/NR/rdonlyres/..._texto_ENG.pdf

Britannia was generally regarded as having 'high standards' within the industry at the time, a long established operator. However deep night flying (a Britannia Airways 'speciality' since inclusive tour charter flying really got going of the 70s) crew fatigue thought a possible contributing factor in this particular 1999 Boeing 757 accident.
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Old 16th Jun 2019, 13:39
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Originally Posted by DaveReidUK
Are you suggesting that some other aircraft are capable of withstanding a similar impact without suffering structural deformation? What type(s) do you have in mind?
I can’t think of any. Not even anything built by Andrei Tupolev. Or
Illyushin.

As as an aside I took a 757 in to Funchal shortly after the Air Europe incident ( our airline stopped 757 operations in to there shortly thereafter). I wandered over to see how the Boeing field engineers ( lots of pens in shirt pockets, crew cuts, and, I suspect, had cut their teeth in ‘Nam) , were fixing it. Jacked up the aircraft by using a pit prop through the dv windows. Drifted the nose gear down and welded it down. Then welded the now deformed window back in to the frame and then an AE crew flew it back gear down ( think they retracted the mains not sure ) to Luton. Built like a brick ****house. As all things Boeing were back in the day.
However there are obviously limits. !! 😎😎😎

Last edited by MENELAUS; 16th Jun 2019 at 14:30.
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Old 16th Jun 2019, 15:43
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Noticing from the images, the starboard thrust reverser is still deployed, but the port is not.
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Old 16th Jun 2019, 17:48
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With regards to the post above, the Britannia incident pushed the dog box up just far enough to snag the thrust lever and reverser cables, but not symmetrically. Looks the same here.

I was, uh, rather close to that particular incident.
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Old 16th Jun 2019, 18:28
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The damaged 757 (I was inside it during the repairs, done by Boeing - Mr Hammer)

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Old 16th Jun 2019, 18:43
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Originally Posted by blue up
With regards to the post above, the Britannia incident pushed the dog box up just far enough to snag the thrust lever and reverser cables, but not symmetrically. Looks the same here.

I was, uh, rather close to that particular incident.
Not quite - there are not 'reverse cables' as such on the 757 - on the 757-200/RB211-535, the throttle cable actuates the reverser Directional Control Valve when it's moved sufficiently aft of forward idle. When the nose gear came back through the EE bay, it snagged the throttle cables in such a way that the engines went to high forward thrust - in that condition it is not possible to deploy the reversers. The combination of high thrust and inability to deploy the reversers made for a rather long overrun.
While the design of using the throttle cables to actuate the reverse DCV was common place back then, it has some highly undesirable failure modes. The 757-300/Rolls didn't use that design (I was directly involved in the design change, including having to debate the Chief Engineer who didn't want to make the change).

In the aftermath, Boeing designed a 'guillotine' system - if the nose wheel came back as it did in Britannia, the guillotine was intended to cut the throttle cables in such a way that the engines would go to idle. I think the guillotine was AD'ed but I wouldn't swear to it.
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Old 16th Jun 2019, 18:52
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Old 16th Jun 2019, 19:23
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Originally Posted by tdracer
Not quite - there are not 'reverse cables' as such on the 757 - on the 757-200/RB211-535, the throttle cable actuates the reverser Directional Control Valve when it's moved sufficiently aft of forward idle. When the nose gear came back through the EE bay, it snagged the throttle cables in such a way that the engines went to high forward thrust - in that condition it is not possible to deploy the reversers. The combination of high thrust and inability to deploy the reversers made for a rather long overrun.
While the design of using the throttle cables to actuate the reverse DCV was common place back then, it has some highly undesirable failure modes. The 757-300/Rolls didn't use that design (I was directly involved in the design change, including having to debate the Chief Engineer who didn't want to make the change).

In the aftermath, Boeing designed a 'guillotine' system - if the nose wheel came back as it did in Britannia, the guillotine was intended to cut the throttle cables in such a way that the engines would go to idle. I think the guillotine was AD'ed but I wouldn't swear to it.
That could have been a double edged sword (sorry...) TD if some poor wight had attempted a go around after initial impact...
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Old 16th Jun 2019, 19:24
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Originally Posted by bafanguy
Anyone interested in waiting until the investigation is complete and facts are in ?
No. What would be the fun in that?

Cheers,
Grog
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Old 16th Jun 2019, 22:52
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Originally Posted by bill fly


That could have been a double edged sword (sorry...) TD if some poor wight had attempted a go around after initial impact...
That was my first thought as well. Hopefully with electronically controlled engines, that failure mode is less of an issue. On to different, newer failures then...
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Old 16th Jun 2019, 23:56
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Originally Posted by bafanguy
Anyone interested in waiting until the investigation is complete and facts are in ?
No. What would be the fun in that?

Cheers,
Grog
I dont see many posts on how it happened, just the results of what happened. They landed hard enough to explode all of the rear landing gear tires and push the nose gear up through the fuselage. No conjecture, it is there in the images.
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Old 17th Jun 2019, 00:32
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Originally Posted by bill fly


That could have been a double edged sword (sorry...) TD if some poor wight had attempted a go around after initial impact...
If you pushed the nose gear far enough into the EE bay to activate the guillotine, attempting a go-around would be a pretty bad decision regardless - the flight control cables go through that same area as the throttle cables (not to mention much of the electronics).
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