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-   -   Incredible recovery of a King Air............ (https://www.pprune.org/private-flying/262947-incredible-recovery-king-air.html)

GotTheTshirt 11th Feb 2007 19:53

Z,
Yes a B200 out of Leavesdon UK on a crew training flight.
Went up to 30+ and did a decompression.
They had mask on but the B200 had the O2 cylinder in the aft fuselage operated by a wire cable from the cockpit.
They put on the masks and opened the valve but the valve on the O2 cylinder had frozen and did not open. the cockpit lever was in the open but the cable "bunched"
The aircraft flew on A/P over the south of England and crashed in Northern France when it ran out of fuel.

GTS

rustle 11th Feb 2007 20:38

September 5, 2000 a King Air flew from Perth (WA) to outback Queensland on autopilot after a pressurisation issue. Level at 25K for 3200+ kms.

See here for ABC report. There will be an ATSB report somewhere, too.

8 dead.

rigpiggy 11th Feb 2007 21:42

not on the KA myself but after this happened, made an extra check on picking up the a/c from another crew. o2 was on but no flow, flights restricted to 13k. a/c in hangar for 1.5 hrs after o2 valve unfroze. fittings disconnected and drained

ChristiaanJ 11th Feb 2007 21:54

Sorry if somewhat O/T.
LOX supply in the F104G, early days (sixties), contamination problems. Similar story, flew for hundreds of miles on A/P before hitting a mountain in Norway. Friend of a friend of mine, so stuck in my memory ever since.

Mark99 13th Feb 2007 05:53

Incredible recovery of a King Air
 
The errors here are too many to even go over.
Crack in windshield - Set cabin to 4.0 psid (Checklist)
Put on mask (that was checked and O2 turned on before takeoff)
Start emergency descent (Checklist)
TUC at FL250? 3-5 minutes
Rate of descent at 180 KIAS (gear speed), between 7 and 8,000 fpm
Time to reach 18,000 - just over a minute
TUC at 18,000 - 30 minutes or more
I think they depressurized (why) and didn't start down. Hence, when the O2 wasn't there, they passed out.
Marvelous tribute to the King Air airframe.
OBW, in the newer B200 (BB1444 and after) the O2 ON handle is on the left of the center console and the Passenger Manual Dropout handle is on the right (right below the Condition Levers).
There's nothing in the NTSB preliminary to conclude anything other than PE.
Sounds almost like the Payne Stewart accident but they lucked out.
Loooooots of KA time, former FSI instructor (Center 32)

AlexEvans 13th Feb 2007 10:14

Can anyone post a working link please?

BRL 13th Feb 2007 12:27

I think this one works

http://www.kfvs12.com/global/video/p...AdTag=homepage

Red Mud 13th Feb 2007 19:35

Here is an excerpt from someone's accounting of the incident:
"Yesterday I was over in Cape Girardeau working on our 170 when a call came
in for an emergency diversion.
Basically, a King Air 200 was on route to Virginia from Arkansas when, at
27,000 feet, the left windshield shattered causing an immediate and rapid
decompression. Given your useful consciousness at this altitude is
measured in seconds, both pilots blacked out. (Fortunately, there were no
passengers on board).
Whether they initiated a rapid descent or lost control and ended up in a
steep dive is not known as the two pilots have little recollection of the
event both fading in and out of consciousness until shortly before landing.
They took turns, unintentionally, of waking up and blacking out and
fighting to regain control of the aircraft. One pilot stated "I remember
thinking we're in a spin and seeing that the airspeed was pegged beyond
indicated. I thought, wow, we're going too fast, reached up and pulled the
power to idle, then blacked out again".
Assume they were pretty much at terminal velocity headed straight down.
At 13,000 feet, (give or take), they started fighting to pull the aircraft
out of a dive. It took both of them. The stress on the airframe must have
been unreal, as you will see.
From that point, parts started leaving the aircraft until landing and they
lost control of pitch. They went almost vertical again and it took both
pilots pushing as hard as they could to get the aircraft to start
descending.
They regained some control around 7,000 feet and were close to cape where
they diverted.
It is fortunate that they did not have a tail stall as you will see, and I
have no earthly idea how they controlled pitch.
There is a God and sometimes he gets your attention to remind you how close
we could all be to standing before him. There is no way this aircraft
could have been flown and landed to a relatively uneventful landing and
they walk away. I cannot explain it and I think you will see what I mean
especially after viewing the empennage.
According to the radar, they lost 20,000 feet in roughly a minute and a
half.
The aircraft is totaled, but again, they taxied to the ramp. Waited a few
hours, and got a car and drove home.
Fortunately, the windscreen did not come in completely, but still should
have most likely been fatal at that altitude."
It sures seems like they weren't in line with any checklist I know of but, not being a King Air guy and not being there, I hesitate to throw too many stones.

exstard 18th Feb 2007 15:15

working link
 
http://youtube.com/watch?v=OWuPmGPBW8o


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