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-   -   Jabiru3602 Engine Failure/Mayday (https://www.pprune.org/pacific-general-aviation-questions/647959-jabiru3602-engine-failure-mayday.html)

blueloo 23rd Jul 2022 07:49

Jabiru3602 Engine Failure/Mayday
 
On Friday Jabiru 3602 declared a mayday with engine failure about 30nm away from Barkley Homestead. Does anyone know the outcome of this ?

tossbag 23rd Jul 2022 23:26

If you want to learn how to deal with an engine failure, hook up with a Jabiru owner. All flying schools should employ at least one Jabiru owner.

If you want a Jabiru, buy a paddock and wait.

Mach E Avelli 25th Jul 2022 02:51

It must be a problem with the plastic airframe.
I owned a Sonex for 10 years. It ran an early Jab 2200 which I think was serial number 65. I flew this thing all over Australia including three Bass Strait crossings. It ran hot, it had no compression, it blew oil out the breather as fast as you could pour it in, the spark plugs were black and sooty and needed changing every 50 hours, and most of the time it was at full throttle, because in my book max continuous power is there to be used. Gentle cruise power is a woftam. It never missed a beat despite once running the oil so low it took almost the full sump capacity to top it up.
Maybe it was the crystals in the metal airframe? If Peter Brock was still with us, he would know.

Styx75 25th Jul 2022 09:42

Then there's this Sonex from January (Jab 3300A)


The aircraft experienced an engine failure after take off. Further inspection revealed that the occurrence was as a result of the flywheel bolts which had become loose.

cooperplace 25th Jul 2022 13:17


Originally Posted by blueloo (Post 11266223)
On Friday Jabiru 3602 declared a mayday with engine failure about 30nm away from Barkley Homestead. Does anyone know the outcome of this ?

Can I ask how you know this? There seems to be nothing anywhere online about this.

Squawk7700 25th Jul 2022 21:17


Originally Posted by Styx75 (Post 11267295)
Then there's this Sonex from January (Jab 3300A)


The aircraft experienced an engine failure after take off. Further inspection revealed that the occurrence was as a result of the flywheel bolts which had become loose.


I hope you’re not suggesting in any way that the above is a fault of the engine?

You can’t compare low compression to loose firewall bolts…

aroa 25th Jul 2022 22:19

Lack of fuel just shy of the destination.? Or drop in pressure of the Thronomeister valve?
If the pilot and a/c ok…good result.

Traffic_Is_Er_Was 26th Jul 2022 03:06


You can’t compare low compression to loose firewall bolts…
Flywheel, not firewall.

Squawk7700 26th Jul 2022 08:00


Originally Posted by Traffic_Is_Er_Was (Post 11267749)
Flywheel, not firewall.

Sorry, fat fingers.

You can’t compare low compression to loose Flywheel bolts.


aroa 26th Jul 2022 21:33

Anyone know the real cause and outcome.?

blueloo 27th Jul 2022 13:25


Originally Posted by cooperplace (Post 11267445)
Can I ask how you know this? There seems to be nothing anywhere online about this.


I (we) heard the mayday call (he was about 100miles away/behind us) - a QF jet relayed for him to ATC on the area frequency. We were transferred to another frequency and didnt hear any further details.

cooperplace 27th Jul 2022 15:15


Originally Posted by blueloo (Post 11268764)
I (we) heard the mayday call (he was about 100miles away/behind us) - a QF jet relayed for him to ATC on the area frequency. We were transferred to another frequency and didnt hear any further details.

Ok thanks. As a jab pilot I'm interested.

cooperplace 30th Jul 2022 09:10

From RAAus:

STATUS: Under review OCCURRENCE DETAILS SUBMITTED TO RAAUS: The Jabiru departed YMKT first light with full wing tanks (135 litres) for a non-stop flight to YBKS. A planned flight time of 5.7 hours. The pilot had been tracking fuel use via fuel flow meter ranging between 13.5 - 15 litres an hour which was as expected, however 27 miles on the 320 radial short of the destination at 2500’ the engine stumbled once and caught again the pilot immediately switched on the electric pump and focused on a landing area on the black soil before flying over a highly treed area that separated the aircraft from Barkley. The engine ran for another 10-15 seconds before winding back to 1250-1300 RPM at full throttle. The pilot had been monitoring the LED fuel lights for the last hour of flight as they were dropping into the red then back to one green bar continuously. They find them notoriously unreliable and always use Fuel Flow Vs take of fuel as my reference. The pilot declared a MAYDAY on area frequency 126.7 and when they received no answer switch to 121.5 and retransmitted the MAYDAY. Response was heard from QANTAS international flight who contacted Brisbane on their behalf. After landing successfully on the desert floor QANTAS handed the pilot over to another aircraft. They do not have the details as all the flight planning and flight log have remained with the aircraft. The pilot of that aircraft stayed in touch with the Jabiru and Brisbane Centre for around 5 minutes. After losing contact with that aircraft on 126.7 the pilot was still unsure if their position was fully known so they activated their beacon and waited for further contact to be made. They tried Brisbane Centre several times with no success and each time transmitted in the blind their position. The pilot tried both area frequency and Brisbane Centre on the hour and half hour times to conserve battery life but received no answer. Approx. 3.5 hours on the ground they heard a helicopter in the distance and contacted it on area frequency to be notified they were coming to assist. R22 landed 5-6 minutes later and remained on the ground at idle until the Jabiru pilot was ready to climb aboard. All they could take was their overnight bag and one Jerry can for fuel. R22 flew them to Barkley Homestead where they spoke to SARWATCH who had contacted the manager by phone. They confirmed there was only 1 POB and the EPIRB was deactivated before they left the landing area. Once on the ground it was immediately obvious that the fuel drain for the header tank had failed open as the last litre had drained onto the desert floor and the remains fuel (approx. 40 litres over 5.7 hours had drained away in flight) at no time did the pilot smell any fuel leak. When the fuel total seemed to be low they visually checked both wing drains and fuel filter clamps and no obvious leak, visual or using smell was present.

blueloo 31st Jul 2022 23:22

Thanks for the update. Glad it was a safe outcome.


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