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tartare
30th Jun 2010, 21:13
See below.
Thoughts?
Another typically aggressive overreaction from NZ it would seem.
Learmount's one of the world's most experienced and respected aviation writers - unlike certain `commentators' here.
Without at all wanting to besmirch the memory of dead men - sadly - it would appear our pilots were suffering from get-home-itis.
There's a lesson in this for all of us.

Air New Zealand has rejected suggestions its crew may have contributed to the crash of an A320 airbus off the French coast almost two years ago.
The five New Zealanders and two German pilots on board were killed when the plane, which was on a test flight, plunged into the Mediterranean Sea near the town of Perpignan on 27 November 2008.
A report by French court-appointed experts concludes the crew lost control of the plane as they tried to perform a low altitude, low-speed test in inappropriate conditions.
Air New Zealand says FlightGlobal website editor David Learmount has claimed the New Zealand crew encouraged the German pilot to perform the manoeuvre in frustration.
It says this claim is baseless and speculative. The airline says the flight recorder shows discussion about the low-speed check happened well before the German pilot began the test at his own initiative.
However, an interim report from French air accident investigators says the New Zealand pilot repeated a request to attempt the manoeuvre three minutes before the crash.

tartare
30th Jun 2010, 22:43
The above reply... a typical case in point.
An organisation characterised by public aggression.
I, like you presumably, am a pilot.
I worked at NZ for many years and know it very well indeed - much, much better than you I suspect.
Read what I posted again... and calm down.
I stand by my post... it was get home-itis that was a contributing factor to this crash... as painful as that may be for people like you to read.

tartare
1st Jul 2010, 00:09
Sorry - I didn't realise how small I was and unknowledgeable I am.
I cower before your grey-headed IFR, multi-engine heavy rated whatever, my big Daddy's yacht driving friend!
Whether it's got one engine or four - big or small - get home-itis still applies.
Good men might be good - but they also make mistakes and bad calls.
And when they're sitting in your seat or mine - good man or not - make a mistake or a bad call and the result's potentially the same - you end up dead.
Don't you think...?

27/09
1st Jul 2010, 00:49
Thoughts?

Yep I have a few.

I think the French are trying to shift the blame. They have a less than stellar record when it come to impartially investigating aviation accidents, plus they have a lot at stake here. (The reputation of Airbus and the work done on the aircraft prior to the fateful flight was done in a French facility.

Regarding the decision to conduct part of the test at low level.

I think it would be fair to say that it was not prudent to carry out the test at the altitude that they did, but certainly not dangerous, under normal circumstances. At least three of the crew (The two German pilots and the Air NZ observer) on board considered it OK to to at that altitude. One has to presume that if any of the the crew thought it a bad idea it would not have taken place.

To try and blame Air New Zealand for this is grossly unfair.


Regarding the faulty sensors.

If these had been working as they should have been the accident would not have happened. Who is to say that even if the aircraft have been at a more appropriate altitude that the crew would have been able to regain control of the aircraft. Look what happened to AF447, it is suspected that faulty sensors might have been the cause of that crash, the aircraft was at cruise altitude and the pilots were unable to regain control. Granted there were possibly min flight speed and Vmo issues to content with.

Tartare
From the tone of your posts, you sound like a disgruntled ex Air NZ employee. Therefore I'm not sure many here will take all of your comments regarding Air NZ seriously.

tartare
1st Jul 2010, 01:10
Now... there is a reasoned response.
Thank you 27/09.
You're the sort of guy I'd feel comfortable flying with.
No - not disgruntled - in the operational part of the business there are a lot of great people at the airline, and I left on good terms.
What I hate is the way they are so corporately, publicly defensive and aggressive - and its an on-going pattern.

mattyj
1st Jul 2010, 01:58
Is this the same investigation team that is taking Continental to court in order to deflect criticism away from Air France's litany of failures in the Conchord case..

eg Takeoff overloaded
Takeoff downwind
Maintenance fails to replace undercarriage spacer

etc

Never let facts get in the way of a good coverup
Concorde crash trial begins - Wikinews, the free news source (http://en.wikinews.org/wiki/Concorde_crash_trial_begins)

buzzz.lightyear
1st Jul 2010, 02:39
Coverup? ANZ wouldn't be involved in coverups would they?
Erebus and financial issues seem to come to mind...

belowMDA
1st Jul 2010, 05:43
I think there has been a lot to learn from this crash, and Air NZ has certainly changed the way it conducts operational flight checks. However, I too remain unconvinced that even if the low speed check been carried out at the recommended altitude the result would have been materially different.

I also really don't like the way the investigation is carried out but unfortunately that's just the way the French do things and I really don't see our condemnation changing anything.

On Guard
1st Jul 2010, 13:01
Regarding the decision to conduct part of the test at low level.

I think it would be fair to say that it was not prudent to carry out the test at the altitude that they did, but certainly not dangerous, under normal circumstances. At least three of the crew (The two German pilots and...

Ummm, no I don't think I would be at all interested in stalling a jet at 3000" on approach, that is so unbeleiveable that there may be more to this story?

Yes this certainly is dangerous under ANY circumstances and should have never been done or asked to be done if indeed this reporting is correct which may not be the case.

Persoanlly I would not do it even at the recommened 6000", 10000: min FL200 pref.

blueloo
1st Jul 2010, 15:36
Does this mean that Airbii can have all the extra unnecessary probes removed as they serve no purpose?

fourholes
1st Jul 2010, 19:55
Biggles.

Fair call. I may have been a tad harsh. I was tired at the time. I have nothing against ppls, and would like to do nothing but encourage their development...and have done over the years. I still believe tartares post to be provocative......and inaccurate...get homeitis? were the boys due home in NZ that night for dinner at 6? seems like a puerile comment to me, to make about professional pilots and engineers. I stand by my comments that the flight was not conducted by Air NZ. It was conducted by XL airways, and had there been a request, or several requests to conduct a low speed test, the decision to do so was, at the end of the day, for the German Captain to decide. I have removed my previous posts.

tartare
1st Jul 2010, 23:17
I didn't intend to be provocative.
Some of you have lost good friends as a result of this - the anger is entirely understandable.
My point r/e get home-itis was more around the focus on achieving a set task within a set time frame causing fixation on that outcome, and becoming one of the human factors in the chain of events that caused the crash.
Tenerife is an example - a highly experienced, multi-engine heavy rated Captain fixating on getting out and home - I've read that accident report in detail.
Anyway - maybe enough said.
Fly safe.

Artificial Horizon
1st Jul 2010, 23:51
Having read through all of the different threads on this subject I think that it is important to fully consider the human factor sides of this event. As a profession we should not be afraid to admit to an accident being primarily attributable to human error. There is no question that there seemed to be some technical faults on this aircraft, but it must not be forgotten that the accident was a direct result of conducting a low speed flight test in a totally inappropriate area at a ludicrous height.

The only explanation for this was the desire to conduct the 'full' acceptance regieme on that sector. It doesn't matter which airlines pilots were flying or not flying, the decision to conduct this test at that time was a poor one, everyone on that flightdeck must shoulder some responsibility for this poor piece of airmanship. Ultimately the PIC must be where the final decision rests but good CRM would dictate that all the flight deck crew also had a responsibility towards allowing this to take place. The aircraft was in the midst of a recovery when it impacted with the water, another few thousand feet as specified in the test outline MAY have made the difference here between a wasteful loss of life and just a bloody scary incident.

Air New Zealand is quite rightly asking for people to wait for the full report before trying to apportion blame, I think that they have to be very careful though because some of the quotes coming out of ANZ do seem to be a bit over the top and sometimes do smack of a company that maybe sticks their head in the sand. I am sure that this is not the case but that is the perception that can develop.

We are all capable of c*cking up, when it is pilot error, we should not be afraid to say so.

fourholes
2nd Jul 2010, 00:45
tartare,

Good points, enough said. artificial horizon, great post.
Lets see what comes out in the official report

Fly safe.

NoseGear
2nd Jul 2010, 02:53
Jeez, a fair, reasonable and measured debate on prune?!?! What the hell is the world coming to?! :}:E
As an Airbus pilot, what test were they conducting? Was it stalling? If so, whats the point in stalling or a low speed test with Airbus protections, or was that the point, to test the protections? Or were the Prims and/or Secs pulled? I haven't read the report if its in there, if anyone has a link?

Nosey

remoak
2nd Jul 2010, 05:44
One of the lessons in this - from the limited information we have so far - is the ease with which 3 experienced and sensible pilots got suckered into an unrecoverable situation. I don't think it was get-home-itis, I am going to assume they were all quite professional enough to not get caught by that one, to me it sounds more like complacency and a perfunctory approach to the task at hand.

Anyway as this is one of those occasions when we really do have to wait for the report before passing judgement, not much more to say on that.

Regarding Air NZ, can we please get past Erebus and Air NZ's past indiscretions? It is a completely different company now. Yes, they do have a monopolistic view of their role in NZ aviation, but the culture seems a lot more professional and open these days. I can still remember the days when wearing glasses was an instant disqualification for pilots looking to join the company... they seem to have moved on.

Regarding the French and their approach to accident investigation, we should be sceptical. There are more politics and pandering going on in the DGAC than is seemly, that's for sure.

compressor stall
2nd Jul 2010, 07:48
Now that the thread has matured, no-one has yet mentioned that late last year Airbus introduced a Technical Flight Familiarisation Course. It's a 5 day course (sim and classroom) pitched at airline pilots doing just such acceptance flights like the tragic one under discussion as these flights go "beyond" what a normal airline pilot would do.

slackie
2nd Jul 2010, 21:50
Anyway as this is one of those occasions when we really do have to wait for the report before passing judgement, not much more to say on that.

WARNING! Someone has hacked into REMOAK's account and is making posts on his behalf!!:ok::}

prospector
2nd Jul 2010, 23:21
Must be a bit of amnesia floating around here.

From NZ Tragedies Aviation by John King.

"Until November 1979 Air New Zealand had not lost a single passenger on a scheduled flight, but it wrote off one-third of its fleet in training accidents."

The Electra ZK-TEC written off at Whenuapai on the morning of 27 March 1965 was a particularly bad so called training practice.

" It's a 5 day course (sim and classroom) pitched at airline pilots doing just such acceptance flights like the tragic one under discussion as these flights go "beyond" what a normal airline pilot would do."

This exercise, with the Electra, as stated in mentioned reference,
" It had absolutely no relevance to anything that might be encountered at any time in airline flying."

So what has been learnt in the intervening years???
The First commandment is still very relevant.

"Thow shalt not make a stuff up or the ground will arise and smite thee"

remoak
3rd Jul 2010, 01:29
WARNING! Someone has hacked into REMOAK's account and is making posts on his behalf!!

Yeah I can't believe I said that... ;)

hoggsnortrupert
3rd Jul 2010, 10:14
Well pray tell Tartare, what are the lessons we can all learn from?

"QUOTE" Tenerife is an example - a highly experienced, multi-engine heavy rated Captain fixating on getting out and home - I've read that accident report in detail. ( well bugger me gently please, so have I, and probably umteen other crews)

SO what is your definition of G.H.I?

You know this tenerife thing, and the Erebus thing keep coming up, and have done for years, with younger crews, and younger lecturers.

Quite frankly both subjects give me the screaming !&its::{:{:{:{

I have never once had Erebus explained as an example in a CRM course as I understand it , and as does alot of NZer's & Aussie's. ( I havnt worked in poverty rocks for years)

As for Tenerife, I feel for poor Capt Van Zanten, all his good gone in an instant with his peer's, so back to my original Question! what is your definition of Get Home Itis?

Havnt been on the boards for awhile! but there is something fishy with Tartare, I fair:

Chr's
H/Snort.:=:=:=:=

Walter E Kurtz
3rd Jul 2010, 23:12
How did both FAC fail at the most critical point during a Normal Law Alpha Max test? The answer to that question is potentially more damaging than the low altitude selected. We must wait for the final report.

balance
3rd Jul 2010, 23:34
Some of you may remember the crash of an ATR-72 at Roselawn in the USA some years ago. The NTSB investigator, Greg Feith, and his team did a remarkable job of figuring out the cause of this accident. In general terms, the accident was caused by ice flowback on the wings, and in some circumstances, could cause the aircraft to become a brick. It came down to a design flaw in the ATR.

Ironically, at a 1996 ISASI conference in Auckland of all places, the Yanks and the Frogs staged a very public argument about who was to blame. The frogs of course, denied that there could ever be a design flaw with their aircraft.

IMHO, the French accident investigators were unreasonable in this case.

This leads me to be very sceptical about ANY investigation carried out by the French. I'm sure they have some fantastic people, but if they let political or financial interests come before air safety, then the basis of any report is clearly compromised.

Just my 2c worth. Hopefully this accident investigation will come to some worthwhile conclusions.

GADRIVR
5th Jul 2010, 00:33
I was going through this thread and wondering when REMOAK would pop up.... and what do we get??
Remoak my lad, you are slipping. Go home, take some nasty pills and have another go. A few of us over here are most concerned about your presumed attack of niceness!!!
:E

remoak
5th Jul 2010, 01:32
I know. I'm pretty ashamed.

Even my kids are concerned that I haven't beaten them with the customary force recently. My wife is in shock after I used the word "please" last week.

I don't know what's happening to my life... :{:{:{

Never mind, I'll be back to normal by the next half-decent thread... :}

43Inches
5th Jul 2010, 02:17
balance,

The ATR had a problem with aileron reversal which was known at design phase to the engineers. They came up with a half fix in 1989 (VGs in front of the ailerons i think) but it was not sufficient to cover the lack of boot protection ahead of the ailerons. In icing conditions a ridge would form aft of the boots and disturb airflow over the ailerons agrevating the reversal problem. The NTSB and French Investigators blamed mostly poor pilot technique in icing prior to Roselawn and it was pilots who kicked up a fuss for years prior regarding the aircrafts unsafe tendancies in icing. Interesting that the engineers were still not listened to as they requested 23% of chord be covered by boots, I think they increased it to 17-18%.

balance
5th Jul 2010, 02:33
Thanks 43 for refreshing my memory. You are quite correct. I've never flown the ATR and couldn't quite remember the details.:ok:

It was interesting though, watching Greg Feith slug it out with the French very publicly at that conference.

I seem to remember an episide of Air Crash Investigations dedicated to this mishap? Was the French reaction mentioned in the episode?

And for that matter, any other Accident Investigators out there had experience with the French?

remoak
5th Jul 2010, 06:09
And for that matter, any other Accident Investigators out there had experience with the French?

Not accident investigations per se, but I have filed a number of incident reports and MORs over the years for events that occurred in French airspace - mostly dangerous mis-communications and ATC actions around Paris CDG - and the airline found it virtually impossible to get a response out of the DGAC. They really do not like admitting that anything might be their fault - part of the culture. Watching the then-head of Airbus defending the A320 following Habsheim is a study in arrogance.

TheShadow
5th Jul 2010, 08:31
Maybe a bit off topic, but (wrt Roselawn crash), I've seen quite a lot of reference to twin turboprop icing "departures" being more to do with the asymmetric buildup of ice on wings (top and bottom surfaces), empennage (including top and bottom of hoz stabs and elevators), nacelles and fuselage caused by the props both rotating in the SAME DIRECTION.

Think about it. Think helix and helical flows. Think the consequences of different (and higher) stall speeds for port and starboard wings.

Ice builds up, autopilot holds wings level until, at the point of stall (at the new much higher Vs), the draggier, most lift-spoilt wing stalls first.

Even if Pilot then de-selects autopilot and valiantly attempts to pick up the dropping wing with aileron (instinctive - BUT always a no-no at the stall, as it embeds you in autorotation), there's no escaping the autorotation/ensuing spin.

Why? Partly because pilot fails to associate his dilemma with having stalled/entered spin and continues to oppose rapid roll with aileron - and partly because the two wings are now of a completely different airfoil shape and drag index spanwise (because of the dissimilar ice distributions).

This type of icing departure occurs mainly in rain-ice/freezing rain (aka SLD). The Feithster's runback ridge and aileron reversal explanation never ever considered this as a factor, but it's been validated in airborne trials.

balance
5th Jul 2010, 08:40
Cheers, Shadow.

http://www.bluecoat.org/reports/NTSB_96_Roselawn_ATR.pdf

43Inches
5th Jul 2010, 09:43
Shadow,

Nothing to do with props,


As the airplane pitched nose up and the AOA increased through 5 degrees, the airflow in the area of the right aileron began to separate from the wing upper surface because of the ice ridge. As the AOA continued to increase, the airflow separation in the area of the right aileron also increased, causing a reversal of the right aileron hinge moment characteristics. Although the right aileron hinge moment reversal caused the ailerons to deflect rapidly to a right-wing-down (RWD) position, the AOA was not sufficient to activate the stall warning system prior to the aileron deflection. The autopilot could not control the aileron deflection rate, which exceeded that allowed by the autopilot so the autopilot disconnected.

Within 0.25 seconds of the autopilot disconnection, the ailerons fully deflected to the RWD position79 and the airplane rolled rapidly to the right until reaching 77 degrees RWD. An immediate nose down elevator deflection reduced the AOA; and the ailerons were deflected LWD by the flightcrew to counter the right roll. The airplane began to roll back towards a wings-level-attitude. The crew then applied 2 to 3 degrees of left rudder and nose-up elevator. The flightcrew's aileron and rudder control inputs reduced the bank angle to 55 degrees RWD. However, as the AOA increased to more than 5 degrees, the airflow over the right aileron separated again, resulting in a second aileron hinge moment reversal and rapid RWD aileron deflection.


This is directly from the NTSB report, it was a flaw in the aircraft design. The flow separation actually commanded the aileron movement not just a simple wing drop stall. The deflection occured at around 180KIAS and only 5 degrees AoA.

The sad part about the whole scenario is that the aircraft had demonstrated aileron hinge reversal on clean airframes during certification at low AOA and they had adjusted the airflow in the area to increase the angle at which it happened. After the first icing related ATR-42 accident in 1987 they knew that it was most probably ice induced aileron reversal and put out a training package and added more VG's to fix the problem. They did not inform any operators or pilots of the findings. The training package did not cover sudden full aileron control deflection with up to 60lbs of force during apparently normal flight (which was what happened in both accidents).

There was a massive lawsuit against ATR because of this.

TheShadow
5th Jul 2010, 12:33
ATR very specifically advised operators that such conditions could effect roll control forces leading to an autopilot disconnect and a resulting roll to a large bank angle until the crew took over the controls. ATR described appropriate recovery procedures and introduced them into ATR training programs. ATR also modified simulator packages for icing operations to simulate such roll departures.
The NTSB knows of the extensive wind tunnel testing, high speed taxi tests, flight testing, and considerable efforts spent by the manufacturer after Roselawn for the first-ever USAF tanker freezing drizzle/rain testing program for civil or military aircraft at Edwards AFB. The NTSB knows from its own involvement in the testing that the phenomenon of an “ice-induced aileron hinge moment reversal” and its associated flow separation behind the boots at low Angle of Attack was discovered for the very first time as a result of this exhaustive post-Roselawn investigation
.
I've re-read the re-issued report for around the fifth or sixth time and I still cannot find anything in there more than the interpretation of uncommanded roll being based upon the specious explanation of runback ice-ridges inducing top surface aileron hinge moment reversal (because nobody had thunk out any other credible explanation).....certainly not the asymmetric icing one leading to a significant (and earlier) stall speed difference between left and right wings.
.
Greg Feith has been associated with a number of facile credible explanations including the 1996 Everglades crash of a Valujet DC9 due to the incendiary effect of poorly stowed (and jostled) oxygen cannisters - despite that airframe's known history of electrical faults, including on the flight preceding its crash - and the grandfathered hazardous wiring insulation type (BMS13-13 aka PVC). Feith is a showman and pretty glib and assertively convincing but also echoes the hollow-man - when it comes down to particularizing the science behind the theory.
.
The problem with icing crash theory is not dissimilar to that of wiring-caused crashes. Post-crash, the evidence is just not there and it takes the tea-leaf readers to colorfully interpret and explain the sparse leads available.
.
But open-minded as always, please do feel free to point me towards anything that's poignantly tantamount to more than assertions of it having been due to "aileron reversal". We all have our belief systems. I just happen to believe that roll departures that are usually (but not always) in the same direction have a common denominator (and that's the L&R prop rotation direction skewing the ice accumulations asymmetrically and thereby favouring a roll to the right i.e. a stbd wing-drop).
.
43 inches said: Within 0.25 seconds of the autopilot disconnection, the ailerons fully deflected to the RWD position79 and the airplane rolled rapidly to the right until reaching 77 degrees RWD. An immediate nose down elevator deflection reduced the AOA; and the ailerons were deflected LWD by the flightcrew to counter the right roll. The airplane began to roll back towards a wings-level-attitude DFDR doesn't (and cannot) discriminate between what was claimed to be aileron snatch and what could have been pilot's instinctive retaliatory input. It's all down to facile interpretation. i.e. Make the data accord with what you think may have happened. Make the evidence fit the mould.

43Inches
6th Jul 2010, 00:12
Here is the evidence trail;

1. Recorder data shows the aileron movement in both accidents, the hinge movement was towards the direction of roll, not against which would be the pilots natural reaction.

2. Certification records from flight testing show cause that aileron hinge reversal occured at low AOA on these aircraft to the point where modifications were carried out (only sufficient for flight in clear or light to moderate icing).

3. During the investigation into the first incident by the ATR & DGAC in 1988 the engineers concluded that aileron hinge reversal could be the cause. This was not promulgated to the NTSB at the time.

4. There was intensive wind tunnel testing of the aerofoil which showed that in extreme icing a ridge would form sufficient to cause aileron hinge reversal which created a force of 50lbs or greater. There was also the famous flights behind the tanker, but these flights could only simulate freezing drizzle not freezing rain. On the second runs made in europe they did find some hinge reversal occured but not to the extent found in the wind tunnel.

5. The most important evidence was from the numerous pilots who had experienced and survived the situation. This had occured over the preceding 10 years where pilots recounted stories of the autopilot disconnecting and the aircraft rolling suddenly with large force required to regain aileron control in icing conditions. After the 1988 incident there was a pilot ban on flying the aircraft in icing but the union gave in when ATR came up with the so called fix.

6. The aircraft was never tested in freezing drizzle or rain conditions as the new european certification rules did not require it to. This was an oversight when the aircraft was put on the FAA register.

The NTSB never created the aileron hinge reversal theory, ATR had known about it the entire time (and pilots of the type). The NTSB was finally able to get at the truth about what happened.

All turbo-props are different and suffer slightly differently in icing, know your aircraft!

framer
6th Jul 2010, 05:47
About the A320 crash;

As with any crash like this there will be many links to the chain and because most people (in the industry anyway) know this full-well, I don't understand why people want to single one out in isolation.
There is a lot to learn from this and I think it would be better to identify a list of what we think the 'causal factors' are and address each one of them.
Here are the things I think need attention based on the interim report;

1/ The test was performed by pilots with no training specific to that test and guided by a pilot with two sim sessions of specific training. (How can the PIC make an accurate assesment of the guidance being offered if he isn't trained for that test) The fact that Airbus have introduced a five day course indicate to me that they think it was a factor, if not in the execution of the maneuver, then in the decision to do it when they did.(would the German Captain have conducted the test at 3000ft if he had completed the five day course?)
2/ XL Airways staff submitted an inaccurate flight plan. This is obviously not what caused the aircraft to crash but I believe it still needs addressing . Do flight plans for 'flight tests' need to be submitted by the PIC? Have airlines cut costs too much in these areas etc.
3/ Europe Aero Services released the aircraft apparently with unservicabilities, what was the error chain within that organisation?
4/The aircraft was intentionally slowed to around 100kts and the test carried out 7000ft below the recommended altitude (shortly after ATC had given them speed control of 180kts), without a clearance from ATC.What combination of commercial pressure, GHI, and ambiguous command environment lead to this action being taken? The Captain was clearly unsure of whether it was wise to do the test but he did it. Why? Thats a CRM PHd right there in itself.

All of these things and probably many others had to occur for the accident to happen in the way that it did (who knows if they would have recovered from 10,000ft), so rather than saying "It was so and so's fault", we should acknowledge that it was a result of many peoples actions or omissions and try to improve the system. Thats what I reckon anyway.
Framer