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Old 3rd Oct 2017, 10:59
  #3820 (permalink)  
Sam Rutherford
 
Join Date: Oct 2007
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It does seem as if the whitewashing continues unabated. We removed the fuel contamination story as untrue (still riding that horse!), looks like Ewald then put it back, we then removed again (after seeing the post here) and now it's been put back again.

Perhaps time to put the (disappeared) crash into the helicopter back on there as well? :-)

Given the FAA report stating "for reasons that could not be determined", it seems a little difficult to maintain the fuel contamination story - but hey, why let the truth get in the way. Ewald has clearly been learning some of the tricks of the trade, and that this thread still has some running to do...

Safe flights, Sam.



NTSB Identification: WPR16LA106
14 CFR Part 91: General Aviation
Accident occurred Wednesday, May 11, 2016 in Winslow, AZ
Probable Cause Approval Date: 12/12/2016
Aircraft: BOEING B75N1, registration: N56200
Injuries: 2 Uninjured.
NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.
The private pilot reported that, earlier in the day, she had flown three flights, totaling about 5 hours of flight time, which included uneventful takeoffs from two airports with a higher density altitude than that which existed at the accident airport; the calculated density altitude at the time of the accident was about 7,223 ft.
The pilot reported that, before takeoff for the accident flight, she conducted an engine run-up and pretakeoff checks, which included leaning the mixture to account for the density altitude. She also conducted a static-power check, which was in the normal range. The pilot reported that, during takeoff for the personal cross-country flight, the airplane accelerated and climbed out normally with the tachometer indicating 2,250 rpm. As the airplane climbed to about 50 ft above ground level, the engine began to lose power, and the airplane started to descend. The pilot turned the airplane left to maintain clearance from obstacles and verified the throttle, mixture, propeller, fuel, and carburetor heat settings. Subsequently, the airplane struck the ground and rolled about 20 ft, the right main landing gear impacted vegetation, and the airplane cart-wheeled. The pilot reported that, just before landing, she observed the tachometer indicating 2,000 rpm.

It is likely that the engine’s partial loss of power, in combination with the high-density altitude, prevented the airplane from being able to maintain a positive climb rate during takeoff. Postaccident examination of the airplane and engine run did not reveal any evidence of any preexisting anomalies that would have precluded normal operation; therefore, the reason for the partial loss of engine power could not be determined.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
• The partial loss of engine power during takeoff initial climb in high-density altitude conditions for reasons that could not be determined because a postaccident examination of the airplane and engine revealed no anomalies.
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