Qatar Airways A330 Dual Engine Flameout
Another website http://www.jacdec.de reports the following.
The funny thing :ooh: is that it quotes PPRUNE as the source. Is something amiss? ----- DATE: 01.06.2006 LOCAL TIME: evening LOCATION: Shanghai-Intl AP (ZSPD) COUNTRY: China AIRLINE: Qatar AW TYPE: Airbus A330-202 REGISTRATION: A7-ACJ C/N: 746 AGE: 0 y + 1 m OPERATION: ISP FLIGHT No.: - FROM: Shanghai TO: Doha VIA: - OCCUPANTS: PAX: - CREW: - FATALITIES: PAX: 0 CREW: 0 OTHER: 0 INJURIES: PAX: 0 CREW: 0 OTHER: 0 DAMAGE TO AIRCRAFT: minor / none After take off, the aircraft suffered a double engine flameout due to unknown reasons. However the pilots managed to restart both engines and returned safely to Shanghai. SOURCE(S): PPRuNe |
Must be some good info on a twin that has both engines shut down during flight, the previous post mentions after take off, I wonder how long after T/O they shut down.???
I remember in the mid/late 80s, a few 757/767s had dual shut downs during flight, think reason was pilots using fuel cock instead off EEC switches during a drill for EEC failure, think Boeing view was just a crew problem. However after a 757 or 767 departing SFO(i think) switched em off at 2500ft, FAA moved quick, temp Mod actioned to have a little plastic or wood block fitted between fuel cocks(not poss to operate both fuel cocks with one hand now) perm Mod to move the EEC buttons away from the fuel cocks. I would like to hear the CVR from the SFO event, I can guess a few words that may of got a mention that day.!!!!!!!!!!!! Any info on this 330 would be good.!!!??? |
On 1 June 2006 an A330-200 aircraft, equipped with GE CF6-80E1 engines, experienced a dual engine flame out during descent around flight level 200. Both engines quickly recovered and a safe landing was performed.
The investigation into this event is being led by the Investigation Authorities with assistance from Airbus. The investigation is in its early stages. An update will be provided when additional information is available and agreed for dispatch by the Investigation Authorities. |
engines were re-lite 2 minutes after initial flame out due to heavy water ingestion.. ( monsoon type rains )
thanx to the auto igintion system of the aircraft and ability to auto start. good machine the 330.. very well protected. |
The GE engines on this 330 were not protected at all from this event - apparently they did indeed flameout. The amount of water ingestion must have been huge (igniters ON - Well beyond any test scenario) or (more likely) no ignition was commanded ON by the aircraft systems.
As I understand it, both the Pratt and GE equipped A330s have new-gen FADECs. For the Pratt equipped A330, there are 5 conditions that will trigger the igniters other than engine start: Anti-Ice ON In-Flight Flame-Out In-Flight Surge TO/GA/Flex Mode Approach Idle Standard OPS would require continuous ignition in this kind of weather condition. Since the A330 has no direct igniter controls, is this accomplished by selecting engine Anti-Ice ON ? And while idle is not the prudent power setting for heavy precip, would not flight idle automatically power the igniters on this aircraft ? |
well.. your right about some of the ignition information.. as for Approach idle.. the ignition will only come on when you have selected flap to position 3 or 4.. on GE and all new 330 aircraft ( as this one was only 2 weeks since delivery ) wing anti-ice does NOT give auto ignition system any more.. althought the ignition can be selected manually..
so far it is assumed that there might have been a failure in the ignition system in general, but that does not explain the quick re-light ( 1 minute for the first engine) airbus sent a team to investigate. |
you can simply put the ignition on by selecting the switch to IGNITION:rolleyes:
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Heard from an A330 driver that they are now advised to set packs to high at top of descent. This advice came out in the last few days which I suspect is related to the event. Are these engines susceptible to compressor stall at low power during descent?
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Originally Posted by Wango Z Tango
so far it is assumed that there might have been a failure in the ignition system in general, but that does not explain the quick re-light ( 1 minute for the first engine)
A jet engine has a continous combustion, so it doesnot need ignition (other than for start or as protection). So how can it fail when it is not even on? The relight(s) only illustrates that the ignition system worked perfect! Very interested in the outcome!! |
Originally Posted by golfyankeesierra
Where does your info come from?
A jet engine has a continous combustion, so it doesnot need ignition (other than for start or as protection). So how can it fail when it is not even on? The relight(s) only illustrates that the ignition system worked perfect! Very interested in the outcome!! I am also very interested as to the correlation between the inflight powersetting conditions (at idle) when they entered the precip vs the engine certification conditions in severe weather. If indeed this is a weather foul-up event |
You may find that this is a carry-on from the same problem on GE equipped B744's with the same suggested fix. W/x conditions are prescribed for the B744 selection of packs, etc., but in a twin [despite 2 being as good as 3 or 4?] it's safer to do it all the time.
G'day ;) |
you can simply put the ignition on by selecting the switch to IGNITION That switch will spring back on ya in another type I am more familiar with. :} I think they will find that it was either buckets of rain beyond anything GE planned for (and certified) or - more likely - there was no ignition being commanded on for whatever reason or - unlikely - the engines were still at idle. |
Am still looking for the first posts on this item, anyone know where they be.
. Still not much info after 8 days, anyone got the info.??? |
Probably not as there is no overhead switch on the bus - well, pack hi flow is, of course. There is combined crank/norm/ignition-or-start switch on the central pedestal and it is not spring loaded in any way.
FD (the un-real) |
Probably not as there is no overhead switch on the bus - well, pack hi flow is, of course. There is combined crank/norm/ignition-or-start switch on the central pedestal and it is not spring loaded in any way. Variety must surely be the spice of life - and I do need to get around a bit more. |
Received Tonight
FROM : AIRBUS CUSTOMER SERVICES TOULOUSE TO : ALL A330 OPERATORS OPERATORS INFORMATION TELEX - OPERATORS INFORMATION TELEX AND FLIGHT OPERATIONS TELEX - FLIGHT OPERATIONS TELEX TO: ALL A330 OPERATORS SUBJECT: ATA 72 - A330 DUAL ENGINE FLAME OUT OUR REF: SE 999.0069/JS dated 09 JUNE 2006 CLASSIFICATION: INCIDENT - ADVICE (FLIGHT OPERATIONS) REFERENCE - OIT SE 999.0067/06/JS dated 02 JUNE 2006 1. PURPOSE The purpose of OIT/FOT is to provide latest update and to provide operational recommendations on the dual engine flame out event reported through OIT ref. SE 999.0067/06/JS dated 02 JUNE 2006. 2. EVENT DESCRIPTION On 1 June 2006 an A330-200 aircraft, equipped with General Electric (GE) CF6-80E1 engines, experienced a dual engine flame out during descent around flight level 200. Both engines quickly recovered and a safe landing was performed. 3. INVESTIGATION STATUS The investigation into this event is led by the Investigation Authorities with assistance from Airbus. The investigation is still in its early stages, however, DFDR preliminary analysis has shown that: - During descent, while engines started to accelerate for aircraft altitude capture, both engines flamed out simultaneously. - Both engines automatically relit after flame out, and recovered within approximately 45 seconds. - Engine Anti Ice had been selected ON during the descent, and Wing Anti Ice had been selected ON shortly prior to the event. - Aircraft systems behavior was normal including automatic RAT extension. Boroscope inspections have been performed on both engines without significant findings. Based on the above, the initial Airbus/GE view is that this event is similar to other power loss events at altitudes above 10 000 ft attributed to inclement weather as experienced on CF6-80 engines installed on various aircraft types. The aircraft returned to service on 7 June 06. 4. OPERATIONAL RECOMMENDATIONS Waiting for final investigation results, in order to increase the fuel/air ratio in the engine so as to mitigate the possibility of experiencing an engine flame out, the following provisional procedure is recommended: ? If inclement weather/icing conditions are expected at any time during descent or if convective activity is identified by the weather radar in the vicinity of the aircraft flight path: At top of descent: - ENG ANTI ICE__ON - WING ANTI ICE_..ON - PACK FLOW___HI Below 10000 feet : Resume normal anti ice and pack flow operation according to weather conditions. Note that the fuel consumption and the idle thrust will slightly increase when selecting ENG ANTI ICE_ON, WING ANTI ICE_ON, and PACK FLOW_HI. Final operational recommendations will be implemented in the FCOM/QRH via OEB or TR. 5. FOLLOW-UP PLAN An update will be provided by 16 June 06. |
Some good info starting to come out.
My thoughts: The now confirmed dual flame-out most probably was due to some external factor. These engines are manufactured to such a degree of precision that their performance, and hence response to external factors, would be identical. An example of this amazing precision is noting that with two (or more :) ) new engines, such as installed on this aircraft (1 month old), the fuel used for both engines, even after long flights will be the same to the nearest KGs, at the most. What may have happened is that the engines encountered a particular condition e.g. quantity of water ingestion, at a specific OAT, at a specific power output and direction (i.e. decel/acel), a specific aircraft speed, specific density ALT etc. that could not be handled by the engines. The incident happened close to an airport, (my assumption since they were in descent), so probably the investigators could even have ground Doppler WX radar records of the event day to establish what the rainfall intensity was at the time. The fix could be something simple as a FADEC 'tweak' to take into account such conditions and more stringent operational recommendations re: flying in inclement weather. Well done to Airbus and GE for producing an airframe/engine combination that recovered brilliantly from what could have been a potentially disastrous scenario and not forgetting the crew, who handled it in a way as not to make headline news! Good stuff :ok: |
from 320DRIVER These engines are manufactured to such a degree of precision that their........performance, Not withstanding the directness of Airbus in illustrating the probable cause and temporary corrective action, I am disturbed that a known problem has migrated from historical service experience into brand new engines on a brand new aircraft. Certainly not very comforting that anybody out there has consulted a lessons learned notebook. Where are the regulators in all this? |
Dump enough water into any fire (including a turbofan), and it will go out. How would you propose the regulators handle this? Prohibit flying in rain?
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Originally Posted by J.O.
Dump enough water into any fire (including a turbofan), and it will go out. How would you propose the regulators handle this? Prohibit flying in rain?
By ensuring that the product can endure an encounter with severe weather to provide freedom from flame out up to no more than one event in 100 million hours. The flip side of this, is how often are you willing to have a multiple engine flame out when flying in rain of unknown quantity? |
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