Go Back  PPRuNe Forums > Aircrew Forums > Military Aviation
Reload this Page >

Stolen military aircraft

Wikiposts
Search
Military Aviation A forum for the professionals who fly military hardware. Also for the backroom boys and girls who support the flying and maintain the equipment, and without whom nothing would ever leave the ground. All armies, navies and air forces of the world equally welcome here.

Stolen military aircraft

Thread Tools
 
Search this Thread
 
Old 9th Jan 2009, 11:01
  #41 (permalink)  
 
Join Date: Aug 2000
Location: uk
Posts: 1,775
Received 19 Likes on 10 Posts
When I was an ATC cadet in the 50's I was told by a couple of LAC's that a Canberra had departed St Athan for delivery to Germany after maintenance. It never arrived and they then discovered that all the paperwork for this aircraft had also disappeared. I always thought that this was a lineshoot but, having read this thread, I am now not so sure.
pulse1 is offline  
Old 9th Jan 2009, 16:09
  #42 (permalink)  
 
Join Date: Jan 2000
Location: sussex
Posts: 347
Likes: 0
Received 0 Likes on 0 Posts
In 1956/7 there used to be three Mosquitos parked at Thruxton facing the
A303 main road which ran alongside the airfield. The story was that they'd been illegally sold to Israel by an ex-WD surplus dealer/scrap man and were intercepted en-route and forced to land at the nearest airfield. I used to drive past them regularly and watched them slowly deteriorate from the fully airworthy aircraft that landed there to wrecks that were ignominiously dragged away a couple of years later and burnt. Very sad. I often wondered who the pilots were and what happened to them ?
virgo is offline  
Old 21st Feb 2009, 02:58
  #43 (permalink)  
 
Join Date: Jan 2009
Location: uk
Posts: 16
Likes: 0
Received 0 Likes on 0 Posts
Not exactly stolen but......

....then there was the groundcrew who 'accidentaly' took-off in a Frightning........'Fortunately' he happened to be a PPL. As he was only supposed to be testing the donks the canopy wasn't fitted....and as the pins were in he couldn't bang-out. Ummm...and the brake-chute was u/s too I recall... However he got it down after a couple of attempts and rather frazzled brakes and tyres - and lived to tell the tale. I think the a/c still exists too.... I always wondered if he had his harness fastened.....and whether he soiled himself.......!
PontiusPilote is offline  
Old 21st Feb 2009, 05:16
  #44 (permalink)  
 
Join Date: Mar 2006
Location: West Sussex
Posts: 1,771
Likes: 0
Received 0 Likes on 0 Posts
Pontius,

The involuntary Lightning ride is definitely true...as I heard it, from several widely spaced but believable sources over the years, the chap did not have a seat or canopy, was sitting on a box !!!

So, no harness, and no chance of a barrier landing.

Reports differ as to whether he had some light aircraft handling experience beforehand.

It took a few attempts to land, including scraping the tail, but he made it.

Sadly, I hope this is wrong but I've also heard this from several sources, the experience affected him very deeply afterwards, basically ruining the rest of his life.

Truly sad after 'getting away' with what most would think a certain death situation, but understandable.
Double Zero is offline  
Old 21st Feb 2009, 05:56
  #45 (permalink)  
 
Join Date: Aug 2007
Location: Chedburgh, Bury St.Edmunds
Age: 81
Posts: 1,175
Likes: 0
Received 7 Likes on 5 Posts
Pontius and Double Zero.
Your facts are almost completely correct. He was an engineering Officer, but he did have RAF wings from a Harvard course many years before this occurrence.
The Lightning concerned is on display in the Aerospace Museum at Duxford.
JEM60 is offline  
Old 21st Feb 2009, 08:49
  #46 (permalink)  
 
Join Date: Nov 2007
Location: East Ecosse
Age: 71
Posts: 453
Likes: 0
Received 0 Likes on 0 Posts
I'll try and find it but I believe he posted here somewhere, detailing the story..




oops wrong forum

Last edited by mustpost; 21st Feb 2009 at 14:24.
mustpost is offline  
Old 21st Feb 2009, 09:35
  #47 (permalink)  
 
Join Date: Jan 2006
Location: In the Doghouse
Posts: 363
Likes: 0
Received 0 Likes on 0 Posts
He was Sqdn Ldr " Taff " Holden, i believe.
sled dog is offline  
Old 21st Feb 2009, 11:18
  #48 (permalink)  
 
Join Date: Aug 2007
Location: Cambridge
Posts: 667
Received 0 Likes on 0 Posts
Sqd Ldr 'Taff' Holden

And the Lightning aircraft he flew now resides in 'Airspace' at IWM Duxford.
Treble one is offline  
Old 21st Feb 2009, 12:10
  #49 (permalink)  
 
Join Date: May 1999
Location: Quite near 'An aerodrome somewhere in England'
Posts: 26,806
Received 270 Likes on 109 Posts
From Lightning XM135, inadvertant flight by W/Cdr Holden - Page 2 - Key Publishing Ltd Aviation Forums

The flight in Taffy's own words

This story is well known in Lightning circles but it is great to be able to hear the real facts 'from the horses mouth' as it were.

Lightning XM135 Inadvertent Flight

Some Background Considerations

In attempting to write a more detailed personal account of my unfortunate flight in Lightning XM135 back in July 1966, I think I should add some of the reasoning and reason why I attempted the test in the first place. This might remove some of the erroneous facts, misapprehensions and misconceptions which I have seen in some accounts of the event.

First I should explain that I was a qualified pilot, even although I was an R.A.F. Engineer Branch officer. I joined the R.A.F. as an apprentice in 1943, from where I gained a cadetship to university. At the university I read mechanical engineering and learnt to fly on Tiger Moths, with the University Air Squadron. On graduation, I was given the option to continue with an engineering career or to follow a General Duties (Flying) career. I chose the former path and the Air Ministry at that time, considered that there was merit in allowing me to qualify to 'wings' standard as a pilot, in the belief that an engineering officer with a pilot qualification, could more easily see the pilots point of view in aircraft maintenance matters. I too, thought this was a very good idea.

I qualified on Harvards, but my early engineering duties only allowed me to keep in flying practice on Chipmunks. Whilst I was at Kinloss, I managed to get checked out on Oxfords and on occasions assisted a qualified test pilot, to air test twin engine Neptunes. My only jet aircraft experience was as a passenger in the second seat of a Javelin T3 and again in the 'rumble' seat of a Canberra. In my service, one of my postings took me to 33MU Lyneham where as the C.O of a civilian manned aircraft storage unit, I had Canberra, Meteor and Lightning types, which were gradually being prepared for despatch to various flying unit tasks. When the Meteor and Canberra types had been cleared, the powers that be, decided that the MU should close after the last Lightning's had been despatched. Up until the last Canberra, I had a qualified and current test pilot on my staff for those aircraft, but he was not a current Lightning pilot. When a Lightning needed test flying, I had to call for any available pilot with a current test pilot rating. Most times I would find one who could be spared within a 24 or 36 hour period. So much for my personal and R.A.F unit background.

Lightning Mk 1A XM135

XM 135 was being prepared for despatch to a Target Facilities Flight, but over a period of weeks, it had been giving no end of trouble. Each time it was being flight tested, the pilot found that on the initial few yards of a take off run, the inverter, supplying power to the primary flight instruments, would cut out and the stand by inverter would have to cut in, clearly an unsatisfactory state of affairs. Electricians were using every trick in their trade to establish the cause, each time thinking that they had removed, replaced and tightened every likely component. With nothing out of order, they would seek another test flight. It was a Boscombe Down pilot who next attempted to fly the aircraft, found the same problem persisting and refused to fly until a more positive explanation could be determined.

Back to the drawing board, electricians decided to devise some tests which might isolate the fault and indicate roughly where and which component was at fault. They intended to ask the next test pilot to switch in and out parts of circuits, using trailing wires from the likely circuits to temporary switches in the cockpit and to do these electrical switchings before and after each few yards of a simulated take off run, when the fault was manifest. The temporary wires from internal circuitry required the cockpit canopy to be removed and in this state the aircraft was made ready for another air test. Being a pilot, it was easiest for me, as CO, to request the services of a qualified test pilot, from wherever I could find one, but for the next test on XM135, no pilot was available for at least another week. With my unit closing down, many civilians being made redundant, a timetable of clearance being upset with this 'rogue' aircraft, there was much tetchiness and irritation amongst my staff. The intended Boscombe Down pilot, knowing I was a pilot, suggested I might try the test myself. He suggested using an out of use runway (Runway36) as I would only be using 30 or 40 yards at a time. He suggested using a Land Rover to communicate with Air Traffic Control and to get their clearance for each movement of the aircraft. However, there was one remaining minor problem. I had only sat in a Lightning cockpit once before and I had no idea how to start its two Rolls Royce Avon engines! The Foreman of engine trades gave me a 5 minute briefing on how to do this and XM135 was towed out to Runway 05 on 22July 1966 for my electrical tests.

It was by way of extraordinary good fortune that my engine Foreman explained that, although I would not be needing reheat, that reheat needed the throttles to be pushed past a reheat 'gate' and one had to feel for the gate keys, behind the throttle, to unlock. My only other knowledge of the Lightning was what I could remember from pilot's notes. At each test flight by the qualified pilot, I would be in ATC with a copy pilot's notes, should he need any aircraft figures to be relayed to him. One or two figures stuck in my mind, namely that the undercarriage had a maximum speed before it should be retracted and I had an even vaguer figure of about 150 knots for a landing speed. Some extra knots would be required for each 1000 lbs. of unused fuel, but I did not need to bother with any such figures for the test, which I was to undertake.

The Ground Test

I was correctly strapped into the cockpit (seated on the in situ parachute and ejector seat) and after starting the engines and holding the aircraft static, on the brakes, I did the necessary preliminaries for the electrical checks in the cockpit, checking the notes I had scribbled on a notepad which lay on the coaming in front of me. All seemed ready for the first test and I indicated to the Land Rover to obtain ATC clearance for use of the short 30 or 40 yards of runway. Holding the brakes I gradually opened the throttles to about 90%. My feeling at the time was the unexpected heavy vibration of Avon power held against the brakes. I did a quick check of the temporary electrical switches and circuitry lights, then released the brakes. That initial punch from the thrust was quite remarkable and I moved the expected 30 to 40 yards before I throttled back and applied the brakes. So far so good. I made some notes, altered some more switch positions, noted the on/off lights and prepared for the next test. This was done in a similar fashion and I was leaving the 'fault' diagnosis to my electrical staff who would have to interpret my notes. I needed to do one more test and ATC had noted that I had only used about 100 yards total, so they were quite happy to clear me for a similar short distance. ATC had also been holding up a fuel bowser and trailer with 3600 gallon of AVTAG for awaiting C130 aircraft refuelling, they decided to allow the bowser to cross the runway. On opening the throttles for that final test, I obviously pushed them too far, misinterpreting the thrust, because of the unexpected heavy vibration and they got locked into reheat. Yes, I did use some expletives but I had no time to think of getting out of reheat, because in front of me, the bowser and trailer had just crossed the runway, from right to left, so my thoughts were to make sure I was missing them by sufficient margin. No, I couldn't steer to clear them; reheat takes you in a straight path like a bullet out of a gun. The time between finding myself in reheat and just missing the bowser was less than half the time I have taken to write this sentence.

Before my thoughts could again return to getting myself out of reheat, I was gathering speed and about to cross the main duty runway, where a Comet had just passed on its take off run. I then had no time to look for reheat gate keys, my eyes were on what next lay ahead. Two things, the end of the short runway 07 and just beyond was the small village of Bradenstoke which I just had to miss. There was no chance of stopping, non whatsoever. I had gained flying speed (that is what reheat is for, short sharp take offs) and I had no runway left. I did not need to heave it off the runway, the previous test pilot had trimmed it exactly for take off and only a slight backward touch on the stick and I was gathering height and speed. Then my thought was to get my speed back in case I should damage the undercarriage. Incidentally, I could not have raised the undercarriage; the ground servicing locks were in place for safety reasons. With only clear blue sky in front of me, I could then search and feel for those gate keys. Yes, I found them and thanked my lucky stars that my engine foreman had quite incidentally told me of their location and I was soon able to get the speed back to (I am guessing now) about 250knots. My next thoughts were to keep Lyneham airfield in sight and where had the Comet got to, the one I had missed a few seconds ago? Then I asked myself, should I eject and where and when? No, I could not; the safety pins were in the ejection seat and safe for servicing, not for flying. My only alternative then was to attempt a landing, but how does one interpolate or extrapolate Tiger Moth, Chipmunk, Harvard flying to a two engined, 11 ton, beast like the Lightning?

After regaining my bearings, a little composure and simply by observation, making sure that the Comet had been warned away, I decided I should attempt a landing on the duty runway and direction. I was trying to combine all my limited flying experience into a few minutes of DIY flight 'training' on a Lightning. It wasn't easy, but I must admit that some of the elementary rudiments of my proper flying training and flight theory were coming in useful. I needed to get the feel of the aircraft, if I was to get it back on the ground. My first approach was ridiculous, I could tell that my speed, height, rate of descent, even alignment wasn't correct and my best plot was to go round again. This time making sure that my throttles would be well below reheat position. A second approach was no better, I had some aspects better, but as the duty runway 25 is on the lip of an escarpment, with a valley floor beyond, my rate of descent took me below runway height and I found myself adding power to get back to the right level. More power also meant more speed and I was trying to get to something like 150 knots for landing, but the uncoordinated attempt was becoming a mess so I abandoned it, took myself away on a very wide circuit of Lyneham and decided to land in the opposite direction. This I thought would give me more time to get the 'feel' right and if I made a mess of the landing, I would overrun the runway and just drop (crash) into the valley beyond. In that direction, with a messed up landing, I would have no fear of crashing into Lyneham village.

The long final leg of this approach gave me the thinking time that I needed and I gradually got the feel that speed, alignment, rate of descent, height and approach angle were better. I plonked it down at about the right position off the runway threshold, but just forgot that I was in a nose wheel aircraft and emulated my best three wheelers in a Chipmunk or Harvard. The result was that I crunched the rubber block which encases the brake parachute cables. However, I had got down, but I then had to stop. I obviously knew the Lightning had a brake parachute, but where was the 'chute lever, button or knob? There, I found it marked Brake Chute and I pulled it and I could then look ahead and concentrate on keeping straight and somewhere near the centre line. I hung on to the brake lever, I wasn't slowing as much as I would like, so I just kept up my hand pressure on the brakes. I had about 100 yards of runway left when I stopped and even then, I didn't know that the brake parachute had dropped off as soon as it was deployed, because the cable had been severed as a result of my super tail wheel three pointer.

Events Immediately after the Flight

XM 135 was towed back to the hangar and I was taken to see the medical officer who gave me some pills to calm my nerves. I felt reasonably calm because I had almost killed myself on five occasions in that 12 minute flight, yet I had miraculously survived. What is more, I would see my wife and young family again. Two or three times in that same 12 minutes, I thought I would never ever see them again. My only priority was to save my own skin, I was not thinking about the non insured loss of a Lightning Mk 1A aircraft. The minor damage to the aircraft was repaired with a new set of brake shoes and a new rubber chute block. As a memento, I have kept that rubber block, one day it might be returned to XM135 at Duxford.

The Fault

Although the tests I did and the ensuing flight did not immediately provide a reason for the initial electrical fault, my electrical staff, with additional assistance from English Electric, Salmesbury eventually did. Apparently, in early versions of the Lightning, there was to be a ground test button fitted into the standby inverter circuit. It was never fitted to the Mk1A but the wires were left in the looms. It was one of these redundant wires which shorted on to the UHF radio as it moved on its trunnions when the aircraft nudged forward on take off. Who would have thought I should risk my life to find it, in the way I did?

Events Subsequent to the Flight

There was a subsequent Inquiry to find out what had happened and why and to make recommendations for it never to happen again. As I was the Commanding Officer of the Unit, I was responsible for my own as well as the service actions of all my staff. I was not acting against any orders in the Flight Order Book which I religiously kept up to date. But those orders did not cater for engineering officers doing investigative type checks on Lightning's. They were later amended. After the Unit Inquiry I had to go up in front of the Commander-in-Chief. That was when I thought my career would be placed in jeopardy. I even thought that my coveted 'wings' would be taken from me; I had no idea how the incident was being regarded by Command or indeed Air Ministry. But, as I stood in front of Air Marshal Sir Kenneth Porter, he read the proceedings, asked me if I agreed with his view that "With the limited flying experience that I had, the test would have been better left to an experienced and current Lightning test pilot." I agreed of course. He then told me to remove my hat, sit down and proceeded to tell me some of his unfortunate flying incidents in Mesopotamia in the Middle East. I was thankful that nothing more was to become of the incident and that I still had a job to do back at 33 Maintenance Unit, Lyneham.

I coped with all the official communications regarding the incident, but what I was unprepared for was the release of the story to the public. I had had very little experience of working with the press, certainly none with radio, TV, national and world press. I had no training in how to deal with their quest for news. My Command Headquarters suggested I went away on leave before press releases were made by Air Ministry. This I did and took my family off camping to Jesola, in Italy. Imagine my complete surprise when, on the first day of camp, on my way to find some ice, someone shouted "Hello Taffy, I've just been reading about your Lightning flight!!" The world seemed a very small place. On returning to the U.K. I was overwhelmed to find that the incident was still front line news. People wanted to write articles in newspapers, books, magazines, interviews on TV and radio and underhand attempts to hear my account of what had happened. Having admitted that I had made an unwise decision to do the ground tests, I decided that the unwanted publicity that I had attracted was in no way going to be for financial gain. I steadfastly refused offers although for a two page article in the Sunday Express, I requested the editors to make a contribution to the R.A.F. Benevolent Fund. Despite prompts, no moneys were ever handed over and I became very disillusioned with all publicity media. Some friends thought I had gained reward for an article in 'Mayfair'; it was written without my knowledge and authority, but, because it was factually correct, I had no redress from the Press Complaints Board. Nonetheless, I was extremely annoyed.

Some years after the incident, my hidden fears of high speed flight came to the surface and I had to spend two periods in hospital. I had not come to terms with the emotional side of the event. To return to my wife and family after five close encounters with death, was indeed a miraculous experience, but I had not been honest with myself, to accept it as such, so I needed psychiatric help. I could recall the technicalities of the flight without any hang-ups, but was unwilling to talk about that emotional side of the ordeal until I was placed under medical drugs and to bring those emotions to the surface. That was a rewarding experience and it gave me a much better understanding of people who might need that same kind of help, after similar unfortunate occurrences.

Forty Years On

I am now retired and living with my wife in Cheshire. Apart from being an active DIY plumber, carpenter, electrician handyman, my main pastime is involvement with family history. My inadvertent flight is still very vivid and in writing this personal account, I needed little prompting. Over the intervening years, I have received many letters and reminders from people whom I did not know, all praising my efforts to return myself and aircraft back to the ground safely. Yes, I have basked in some glory, when accounts of what happened, have been retold in social gatherings. I have never sought publicity, but whenever it became impossible to suppress, I have had to live with it. I enjoyed my career in the Royal Air Force, but not because of XM135!

Best regards

Taffy Holden
BEagle is online now  
Old 21st Feb 2009, 15:07
  #50 (permalink)  
 
Join Date: Mar 2006
Location: West Sussex
Posts: 1,771
Likes: 0
Received 0 Likes on 0 Posts
Lightning ride

Beagle,

Thankyou very much for putting up the true account, I for one always felt I was being told something near but not quite the reality.

As for Mr.Holden, I don't think I've ever read a more humbling story - a very brave, and honest man.

I suppose, in modern parlance, ' Respect ' Sir !

DZ
Double Zero is offline  
Old 21st Feb 2009, 19:29
  #51 (permalink)  
 
Join Date: Feb 2009
Location: North East Scotland
Posts: 9
Likes: 0
Received 0 Likes on 0 Posts
Lightning Ride

I've observed this forum for years and never felt the urge to pass comment, until today.

I first heard this story when I joined the RAF in 1985 and, at first, dismissed it as bull***t. Then I heard it again and again and again, so realised there must have been a grain of truth to it and, if I'm honest, I was in awe of it.

Thanks for posting Taffy's account of this. Its good to finally know the true events.
The Magic Rat is offline  
Old 21st Feb 2009, 19:41
  #52 (permalink)  
 
Join Date: Jun 2004
Location: Lincs
Posts: 2,307
Received 0 Likes on 0 Posts
BBC radio interview with Wing Commander Holden. Recorded in the 1980s.

YouTube - Lightning XM135 inadvertant flight by W/Cdr "Taffy" Holden

TJ
TEEEJ is offline  
Old 21st Feb 2009, 19:49
  #53 (permalink)  
 
Join Date: Jun 1999
Location: Lost
Posts: 387
Received 4 Likes on 4 Posts
NutherA2 - great dit.

Bit off-thread this next bit:

I seem to remember be told a dissimilar story by a Gp Capt Nav (Gp Capt Cadets at Cranwell in 1990??) who, as an FO on 9 Vulcans, helped nick 617's bit of the Tirpitz. As they got airborne they got a Grade One div back to Scampers. They declared a Mayday with an engine fire indications (false), divved into Wittering, shut down in the bondu and chucked the scrap iron over the hedge. He went back that night in his motor and re-acquired it for the squadron. OC 9 very happy. OC 617 less so. Or was it the other way round?

I seem to remember that forgetting to sign the 700 was deemed to be "stealing of of Her Majesty's aircraft". In which case I wise to have several dozen cases taken into consideration.
Dunhovrin is offline  
Old 22nd Feb 2009, 05:54
  #54 (permalink)  
 
Join Date: Aug 2007
Location: Chedburgh, Bury St.Edmunds
Age: 81
Posts: 1,175
Likes: 0
Received 7 Likes on 5 Posts
Ah, yes. This brought back memories. Story of 'bulkhead' was told to me by Vulcan Capt. K. D.....n whilst climbing for a spinning excercise whilst instructing me for a PPL. Many years ago!!
JEM60 is offline  
Old 22nd Feb 2009, 12:16
  #55 (permalink)  
 
Join Date: Sep 2005
Location: Norfolk UK
Age: 80
Posts: 1,200
Likes: 0
Received 0 Likes on 0 Posts
C130

I'm not military but am a PPL.
We used to keep a sailing boat at Aldeburgh ,Suffolk and I sometimes took a couple of USAF pilots sailing,in turn I would get invited to the Officers mess at Bentwaters for a meal,first time I tasted a real burger!
Also saw round much of the Bentwaters base and Woodbridge.
I asked them about this 130 episode and whether the USAF shot it down,they never said anything,just gave a rather knowing smile.

One of the groundcrew I used to see in the pub told me there was no way they were going to let it crash on land and cause a serious international row.
Lister
Lister Noble is offline  
Old 22nd Feb 2009, 12:50
  #56 (permalink)  
 
Join Date: May 2002
Location: UK
Posts: 1,195
Received 10 Likes on 7 Posts
I seem to remember be told a dissimilar story by a Gp Capt Nav (Gp Capt Cadets at Cranwell in 1990??) who, as an FO on 9 Vulcans, helped nick 617's bit of the Tirpitz. As they got airborne they got a Grade One div back to Scampers. They declared a Mayday with an engine fire indications (false), divved into Wittering, shut down in the bondu and chucked the scrap iron over the hedge. He went back that night in his motor and re-acquired it for the squadron. OC 9 very happy. OC 617 less so. Or was it the other way round?
Err no. The 9 squadron crew arrived at Waddington an a UK ranger. The captain, P**e A*ms****g, approached me in the briefing room and asked if I knew a place where he could hire a van. I thought nothing of it and suggested a couple of local companies. That evening the the station was "invaded" for want of a better term, by 617 sqn who were seeking the return of "their property". The Waddington residents decided that this was a 617/9 spat and declined to get involved, sitting back to watch the entertainment. Nothing was found and I am pretty sure that the 9 sqn crew had already made themselves scarce. When the 9 sqn aircraft was due to depart for Akrotiri (next morning?) a search was carried out but revealed no rusty old bits of battleship secreted on board. They got airborne and straight away diverted to Cottesmore or Wittering (cannot recall which) where they refuelled and loaded the pre-positioned scrap iron and then departed for Akrotiri.

The tale of the subsequent 617 "mission" to reacquire the old bit of boiler plate is even more entertaining, but as I have only had it related to me 2nd hand I shall not re-tell. I shall try and get a friend who was on Bomber Wing at the time to provide an account.

YS
Yellow Sun is offline  
Old 27th Feb 2009, 03:59
  #57 (permalink)  
bho
 
Join Date: Apr 2008
Location: New Mexico
Posts: 2
Likes: 0
Received 0 Likes on 0 Posts
LCpl Foote

I heard a rumor that after LCpl Foote got bounced out of the Corps he ended up flying for the Israeli Air Force. Anybody know what became of LCpl Foote?
bho is offline  
Old 27th Feb 2009, 04:26
  #58 (permalink)  
Thread Starter
 
Join Date: Jul 2006
Location: by the Great Salt Lake, USA
Posts: 1,542
Likes: 0
Received 0 Likes on 0 Posts
Well, this seems to be him (second entry).

There is an error in the article, it says he enlisted in the USMC in 1994 and became a plane captain on A-6E Intruders... the USMC got rid of its last A-6E squadron in 1995... about the time he would be finishing training.

Note the other dates, though... enlisting in 1984 fits those dates much better (I doubt he was contracting with NASA's JPL while an enlisted man in the USMC)... as well as the Foote of "stolen Skyhawk" fame.

Management Profile: Alchemy Enterprises, Ltd.
GreenKnight121 is offline  
Old 27th Feb 2009, 06:23
  #59 (permalink)  
 
Join Date: May 1999
Location: Quite near 'An aerodrome somewhere in England'
Posts: 26,806
Received 270 Likes on 109 Posts
YS, the version I heard was that the ac left Waddo with Akrotiri fuel, but landed over normal landing weight at Wittering. Then loaded the bit of boat whilst the 617th bombardment wing were racing down the A1 - and took off again.
BEagle is online now  
Old 27th Feb 2009, 10:08
  #60 (permalink)  
 
Join Date: Nov 2008
Location: Exit stage right.
Posts: 290
Likes: 0
Received 2 Likes on 2 Posts
Beagle,

Thankyou very much for putting up the true account,
I agree

Would be great if the museum had a piece by the exhibit which detailed this as gives a lot more feel to an exhibit knowing what the aircraft was involved in and some of what the people have been involved with.
racedo is offline  


Contact Us - Archive - Advertising - Cookie Policy - Privacy Statement - Terms of Service

Copyright © 2024 MH Sub I, LLC dba Internet Brands. All rights reserved. Use of this site indicates your consent to the Terms of Use.